I WAS DRIVING UPHILL ON HIGHWAY 152 WHEN MY SLIP YOKE EXPLODED BLOWING OUT THE REAR OF THE BELLHOUSING TO MY TRANSMISSION THROWING THE TRUCK REAR END 6 FT IN THE AIR AND THE NOSE OF THE TRUCK 3 FEET IN THE AIR THIS WAS CAUSED BY THE DRIVE SHAFT TAKING INTO THE GROUND WHEN COMING DOWN THE DRIVESHAFT SLAPPED AROUND RIPPING OUT THE EXHAUST MANIFOLD FROM THE CADILLAC CONVERTER AND PUT A LARGE GASH APPROXIMATELY 12IN TO 18 IN INTO THE GAS TANK WHEN I DROP MY TRANSMISSION TO REPLACE IT I FOUND OUT THAT THE BLOCK WAS NO GOOD DUE TO THE FACT THAT 2 SQUARE PIECES OF THE BLOCK APPROXIMATELY 2 IN SQUARE CAME WITH THE TRANSMISSION AS IT WAS PULLED LEAVING THE BLOCK USELESS BUY THIS SLIP YOKE EXPLODING WHICH I FOUND OUT ON YOUTUBE THIS HAD HAPPENED TO OTHER FORD RANGERS OF THIS PARTICULAR YEAR DUE TO THE FACT THAT THE SLIP YOKE IS MADE OUT OF COMPRESS MATERIAL IT SHOULD BE A SOLID STILL PEACE IF NOT FOR GOING UPHILL I'M SURE MY TRUCK WOULD ROLLED END-OVER-END INN MAKING THIS INCIDENT FATAL IF I HAD KNOWN I COULD HAVE MADE AN INSTANT DIDN'T REPORT ABOUT THIS SITUATION EARLIER I WOULD HAVE
2 injured
1988 FORD RANGER WAS TOWED BACK OUT HERE ON 4/1/2011 OK THIS 1988 FORD RANGER HAS NOT BEEN DROVE ANYWHERE OK IT ALSO WAS ON RECALL FOR BRAKE WORK AN THIS CAN'T BE DONE EITHER CAUSE OF OTHER ISSUE WITH POWER TRAIN AN YOU NEED BRAKE AN BE ABLE TO USE THE CLUTCH AS WILL OK AN THIS IS SITTING IN THE SIDE OD THE DRIVEWAY HERE THE 1988 FORD RANGER HAS X OUT RECALL RIGHT WITH THIS VIN NUMBER [XXX] , AN WHILE THEY WAS WORKING ON THIS 1988 FORD RANGER THERE WAS DAMAGE DONE , THEY NEVER PUT THE PART BACK AT ALL THERE BIG WHOLE THERE THIS 1988 FORD RANGER WAS A TRADE IN AT FAIRWAY FORD IN FREEPORT IL ON 2003 FORD RANGER. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TR
1988 FORD RANGER STILL NEEDING A NEW CAB, WELL I WENT ONLINE HERE TO SEE IF I COULD FIND SOME WHERE TO GET A 1988 FORD RANGER CAB. SO CHATTING ONLINE HERE WITH WHOLE SALE FORD RANGER SARA ASKED ME FOR A PART NUMBER FOR THE NEW CAB I SAID THAT THEY NEVER GAVE ME ONE ON THE RECEIPT. I CALLED SOME WHERE ELSE OK BRAD IS NAME AND HE SAID THAT I COULD PUT A PARCH IN THERE WHERE IT WOULD BE ROAD SAFE . BODY SHOP WOULD HAVE MY FORD RANGER BACK TO ROAD SAFE. OK, WHAT'S THE HOLD UP ON THIS NOW ? I MAILED IN THE EVERYTHING THAT WAS SAID. UPDATED IVOQ 08/05/10 UPDATED IVOQ 08/19/10*JB *TR
DRIVING 60 MPH, A LOSS OF POWER WAS NOTICED. THIS BECAME A LOUD EXHAUST NOISE. AFTER COASTING TO A STOP, PUTTING UP THE HOOD TO SEARCH FOR PROBLEMS, AND FINDING NO EVIDENCE OF ANY, ATTEMPTED TO RESTART THE VEHICLE. THE VEHICLE BACKFIRED, AND SMOKE BEGAN TO POUR OUT FROM THE EXHAUST SYSTEM. A FIRE STARTED WHICH COMPLETELY DESTROYED THE VEHICLE. *TR
Fire
WENT TO PICK UP MY 1988 FORD RANGER TODAY AT FAIRWAY FORD FREEPORT IL AT NUMBER 1 815 232 6868 OK I WAS TOLD HERE THAT THEY HAD BEEN TRYING TO CALL ME BUT WAS UNABLE TO REACH ME CALL HAD WRONG PHONE NUMBER OK BUT I HAVE REPORT HERE THAT STATE THAT TO FIX 1988 FORD RANGER THE FIRE WALL IS UNFIXABLE THEY NEW CAB TO MATCH THE COLOR OR APAINT JOB EITHER WAY AND I WILL SETTLE ON THIS PLU THEY WILL FIX MY CHEVY FOR PART THAT WILL BUY THAT NEED TO FIX WITH , BUT THEY NEED TO KNOW TO WHERE FINE ONE AT THAT IS ROAD SAFE, THAT YOU WOULD APPROVE AN THEY WILL REPAIR THE 1988 FORD RANGER AT THERE COST. *TR
I BOUGHT A 1988 FORD RANGER TAN GOLD IN COLOR LOVE THE TRUCK, BUT I WENT TO INDIANA TO PICK MY SON UP EVERYTHING WAS FINE BUT ON THE WAY BACK THAT'S WHEN EVERYTHING STARTED TO FALL APART HERE. OK, STARTER WOULDN'T RESTART HAD TO POP CLUTCH IT, AN THEN THE CLUTCH PEDAL ITSELF GAVE AWAY FROM THE FIRE WALL ON THE WAY HOME TO SAVANNA IL. OK, IT WAS DARK OUT SO THE NEXT DAY WENT TO LOOK AND MY SON AND I SAW THERE WAS A CRACK THERE SO WE TRIED TO FIX THIS AN SEE WHY IT WASN'T STARTING UP. I CALLED MIDAS TO SEE IF THEY WOULD WELD THIS UP FOR ME. WE HAVE TRIED CARPENTER TAPE TO TRY AND PULL THE FIRE WALL BACK IN TO RELEASE THE CLUTCH TO GET THIS TRUCK SOMEWHERE TO BE FIXED AT THE FORD DEALERSHIP IN FREEPORT IL , BUT I HAVE CALLED ON FORD TO DO SOMETHING AND NOT WAIT ON AN ACCIDENT OR RECALL. THE FLUID THAT LEAKED OUT HIT THE MOTOR GOING DOWN THE ROAD. UPDATED 5/12/10 *CN UPDATED IVOQ 05/26/10 ACCORDING TO THE SERVICE INVOICE. THE FIRE WALL COULD NOT BE REPAIRED DUE TO THE CONDITION IT WAS IN. THE DEALER RECOMMENDED A NEW CAB. UPDATED IVOQ 07/13/10 UPDATED 07/15/10.8JB *TR
I BOUGHT A 1988 FORD RANGER TAN GOLD IN COLOR LOVE THE TRUCK, BUT I WENT TO INDIANA TO PICK MY SON UP EVERYTHING WAS FINE BUT ON THE WAY BACK THAT'S WHEN EVERYTHING STARTED TO FALL APART HERE. OK, STARTER WOULDN'T RESTART HAD TO POP CLUTCH IT, AN THEN THE CLUTCH PEDAL ITSELF GAVE AWAY FROM THE FIRE WALL ON THE WAY HOME TO SAVANNA IL. OK, IT WAS DARK OUT SO THE NEXT DAY WENT TO LOOK AND MY SON AND I SAW THERE WAS A CRACK THERE SO WE TRIED TO FIX THIS AN SEE WHY IT WASN'T STARTING UP. I CALLED MIDAS TO SEE IF THEY WOULD WELD THIS UP FOR ME. WE HAVE TRIED CARPENTER TAPE TO TRY AND PULL THE FIRE WALL BACK IN TO RELEASE THE CLUTCH TO GET THIS TRUCK SOMEWHERE TO BE FIXED AT THE FORD DEALERSHIP IN FREEPORT IL , BUT I HAVE CALLED ON FORD TO DO SOMETHING AND NOT WAIT ON AN ACCIDENT OR RECALL. THE FLUID THAT LEAKED OUT HIT THE MOTOR GOING DOWN THE ROAD. UPDATED 5/12/10 *CN UPDATED IVOQ 05/26/10 ACCORDING TO THE SERVICE INVOICE. THE FIRE WALL COULD NOT BE REPAIRED DUE TO THE CONDITION IT WAS IN. THE DEALER RECOMMENDED A NEW CAB. UPDATED IVOQ 07/13/10 UPDATED 07/15/10.8JB *TR
I BOUGHT A 1988 FORD RANGER TAN GOLD IN COLOR LOVE THE TRUCK, BUT I WENT TO INDIANA TO PICK MY SON UP EVERYTHING WAS FINE BUT ON THE WAY BACK THAT'S WHEN EVERYTHING STARTED TO FALL APART HERE. OK, STARTER WOULDN'T RESTART HAD TO POP CLUTCH IT, AN THEN THE CLUTCH PEDAL ITSELF GAVE AWAY FROM THE FIRE WALL ON THE WAY HOME TO SAVANNA IL. OK, IT WAS DARK OUT SO THE NEXT DAY WENT TO LOOK AND MY SON AND I SAW THERE WAS A CRACK THERE SO WE TRIED TO FIX THIS AN SEE WHY IT WASN'T STARTING UP. I CALLED MIDAS TO SEE IF THEY WOULD WELD THIS UP FOR ME. WE HAVE TRIED CARPENTER TAPE TO TRY AND PULL THE FIRE WALL BACK IN TO RELEASE THE CLUTCH TO GET THIS TRUCK SOMEWHERE TO BE FIXED AT THE FORD DEALERSHIP IN FREEPORT IL , BUT I HAVE CALLED ON FORD TO DO SOMETHING AND NOT WAIT ON AN ACCIDENT OR RECALL. THE FLUID THAT LEAKED OUT HIT THE MOTOR GOING DOWN THE ROAD. UPDATED 5/12/10 *CN UPDATED IVOQ 05/26/10 ACCORDING TO THE SERVICE INVOICE. THE FIRE WALL COULD NOT BE REPAIRED DUE TO THE CONDITION IT WAS IN. THE DEALER RECOMMENDED A NEW CAB. UPDATED IVOQ 07/13/10 UPDATED 07/15/10.8JB *TR
DT*: THE CONTACT STATED WHILE DRIVING 20 MPH IN DOWNTOWN TRAFFIC AND DEPRESSING THE BRAKE PEDAL, THE VEHICLE WOULD NOT STOP. THE VEHICLE WAS MANEUVERED AROUND TRAFFIC AND COASTED TO A STOP ON A SIDE STREET. THE CONTACT CHANGED THE BRAKE LINES AND THE DEALER WAS NOT NOTIFIED.
DT: THE CONTACT STATED 1988 FORD RANGER CAUGHT ON FIRE ON JULY 28 ,05. IT BURNED UP ALL OF THE WIRING, ENGINE, AND ONE TIRE. THE FIRE ORIGINATED FROM UNDER THE HOOD. THE CAR HAD BEEN SITTING FOR ONE YEAR. THE CONSUMER HAD BEEN WORKING ON THE CAR. HE REBUILT THE TRANSMISSION, PUT A NEW REAR END UNDER IT, AND PUT ON OXYGEN SENSORS. HE ATTEMPTED TO RESTART VEHICLE AND IT QUIT. HE WENT TO START IT AGAIN IT BACK FIRED AND CAUGHT ON FIRE. HAS NOT CONTACTED FORD ABOUT THE FIRE. HE SEEMED TO THINK THE FIRE WAS FUEL RELATED. *AK
Fire
DT: THE VEHICLE CAUGHT ON FIRE ON THE ENGINE BY THE FUEL RAIL. FIRE DEPARTMENT CAME AND EXTINGUISHED THE FIRE. THIS HAPPENED ON JULY 26, 2005. THE VEHICLE HAD BEEN PARKED FOR SEVERAL MONTHS. TRIED TO START IT THEN IT BACK FIRED AND CAUGHT FLAMES. *AK
Fire
FAILURE IN THE IGNITION SYSTEM (THIRD TIME WITH THIS VEHICLE) 2-12-97 WAS THE FIRST TIME I REPLACED THE IGNITION MODULE, THEN ON 10-01-01 THE IGNITION MODULE NEEDED TO REPLACED A SECOND TIME. THIS IS QUITE A CONCERN TO ME BECAUSE THE VEHICLE COMPLETELY STALLS OUT. I LOSE ALL POWER, INCLUDING STEERING. THE MOST RECENT FAILURE WAS WHEN I WAS DRIVING HOME ON THE 55 FREEWAY DOING ABOUT 60 MPH. THIS FAILURE ALSO DAMAGED THE DISTRIBUTOR WHICH ALSO HAD TO BE REPLACED*AK.
WHILE TRAVELING ON THE HIGHWAY HEADLIGHTS STARTED FLICKING ON AND OFF. CONSUMER TURNED THE VEHICLE OFF AND IT CAUGHT ON FIRE UNDERNEATH THE HOOD. *AK
Fire
CONSUMER STATES WHILE DRIVING THE VEHICLE THE IGNITION SWITCH CAUGHT ON FIRE, VEHICLE WAS PULL OUT THE ROAD. DEALER HAS BEEN NOTIFIED. IF YOU HAVE ANY ADDITIONAL INFORMATION FEEL FREE TO ADD. NLM
Fire
ALL FOUR OVERLOAD SPRINGS USED ON TWO DIFFERENT PICKUP TRUCKS USED AS PAINTER'S WORK VEHICLES HAVE FAILED IN THE PAST THREE OR FOUR YEARS. EACH TIME AN EIGHT INCH CHUNK OF HARDENED STEEL SPRING WEIGHING AT LEAST A COUPLE OF POUNDS HAS BLASTED LOOSE RICOCHETING DOWN THE HIGHWAY. SO FAR NONE OF THESE FAILURES HAVE CAUSED ME AN ACCIEDNET, BUT WITH A 100% CATOSTROPHIC PRODUCT FAILURE RATE I WOULD IMAGINE OTHERS HAVE NOT BEEN AS FORTUNATE. CAMPWAYS SHRUGGED IT OFF WITHOUT INTEREST. BOTH TRUCKS HAVE ALWAYS BEEN USED WELL WITHIN NORMAL URBAN WORK TRUCK PARAMETERS. IN MY OPINION THESE OVERLOAD SSPRINGS PRESENT A CLEAR, POTENTIALLY FATAL VEHICLE SAFETY HAZARD.
WHILE TRAVELING APPROXIMATELY 70 MPH IN A 1988, FORD TRUCK, RANGER, A FIRESTONE FR480 TIRE , SIZE: P215/70R14, DOT: W2HYFR5106 EXPERIENCED TREAD SEPARATION. THERE WERE APPROXIMATELY 30,000 MILES ON TIRES, AND IT WAS NOT ORIGINAL EQUIPMENT. *AK CONSUMER STATED THAT, FIRESTONE CUSTOMER AFFAIRS CONTACTED DEALER WHO REPLACED HIS TIRE AT MINIMAL COST. *YD
ENGINE RUNS TOO FAST WILL NOT IDLE -AIR COMPRESSER WILL NOT WORK. *AK
ENGINE RUNS TOO FAST WILL NOT IDLE -AIR COMPRESSER WILL NOT WORK. *AK
INTERMITTENT SUDDEN ACCELERATION WHEN STARTING VEHICLE. VEHICLE BEEN TO DEALER SHOP ON THREE OCCASIONS, AND WAS UNABLE TO DUPLICATE THE PROBLEM. FEEL FREE TO PROVIDE ANY FURTHER INFORMATION ON THIS MATTER.*AK
REAR BRAKES LOCK UP AFTER VEHICLE HAS SET OVERNIGHT AND ESPECIALLY DURING DAMP WEATHER. *AK
MY HUSBAND WAS EAST BOUND ON HWY 90 BY RITZVILLE, WA WHEN HIS FORD RANGER WENT OFF THE ROAD FOR NO REASON (ACCORDING TO WITNESSES AS HE HAD JUST PASSED A TRUCK) THE TRUCK ROLLED, SEAT-BELT FAILED AND HE WAS THROWN FROM THE TRUCK. WE HAVE HAD LOTS OF PROBLEMS WITH THIS RANGER AND OUR BRONCO II STALLING OUT AT ROAD SPEEDS. I BELIEVE THIS IS WHAT HAPPENED TO MY HUSBAND. ACCORDING TO THE INVESTIGATING POLICEMAN, THERE WAS NO EVIDENCE OF ANYTHING WRONG WITH THE TRUCK SUCH AS A BLOWN TIRE, BROKEN TIE-ROD, ETC. THIS ACCIDENT OCCURED ON A STRAIGHT STRECH OF ROAD IN THE EARLY AFTERNOON UNDER GOOD WEATHER CONDITIONS. I HAVE A NUMBER OF REPAIR AND REPLACEMENT RECIEPTS RELATED TO THIS STALLING PROBLEM. AS WELL AS A BRONCO II THAT STILL STALLS AT HIGHWAY SPEEDS! PLEASE HELP BY INVESTIGATING THIS PROBLEM.*AK
Crash
1 deaths
VEHICLE WAS PARKED, KEY WAS NOT IN IGNITION AND IT WAS IN GEAR , IT CAUGHT FIRE AND ROLLED ABOUT 50 FT WHERE IT HIT A BUILDING. $ AMOUNT OF DAMGE NOT KNOWN AT THIS TIME. *AK
Fire
TRANSMISSION VIBRATES AND MAKES A LOT OF NOISE- GEARS SOUND LOOSE. *AK
THIS PROBLEM OF THE ENGINE SUDDENLY STOPPING FIRST OCCURRED DURING THE SUMMER OF 1990. I WAS ON INTERSTATE 70 DRIVING TO IN THE MOUNTAINS WHEN THE ENGINE SUDDENLY STOPPED. THIS WAS THE FIRST OF A SERIES OF ENGINE SHUTDOWNS THAT HAVE OCCURREDS CONTINUALLY SINCE THAT FIRST INCIDENT. THE SHUTDOWNS HAVE OCCURRED AT SPEEDS RANGING FROM 25 MPH TO 75 MPH. THE USUALLY HAVE OCCURRED AT THE HIGHER SPEEDS ON A HIGHWAY DURING WARMER WEATHER, BUT THEY HAVE ALSO OCCURRED AT LOWER SPEEDS IN THE CITY---ALTHOUGH LESS FREQUENTLY. WHEN I FIRST CHECKED WITH A MECHANIC ABOUT THE PROBLEM I WAS TOLD THAT IT WAS PROBABLY THE FUEL FILTER. REPLACING THESE DID NOT SOLVE IT. I ALSO HAD THE VEHICLE TUNED HOPING THAT WOULD SOLVE IT. SEVERAL TUNE UPS HAVE NOT HELPED. FINALLY, IN 1996 I WAS TOLD BY A FORD TRRAINED TECHICIAN WHOM I MET WHILE ON VACATION THAT IT WAS PROBABLY THE TFI MODULE. JUST THIS SEPTEMBER I DECIDED TO HAVE THE UNIT REPLACE ( I HAD FOUND A GOOD FORD TRAINED MECHANIC WHOM I HAD BEEN TAKING THE VEHICLE TO FOR SERVICING AND A MINOR REPAIR THE PAST YEAR). HE REPLACED THE ORGINAL TFI MODULE AND THE STATOR ASSEMBLY WITH FORD FACTORY PARTS---TFI MODULE E6SZ-12A297-A AND THE STATOR ASSEMBLY E8PZ-12A112-A). TWO DAYS AFTER REPLACING THESE PARTS THE ENGINE QUITE WHILE DRIVING ABOUT 30 MPH IN DOWNTOWN BOULDER, CO. I DID NOT LEARN THAT THE CAUSE OF THE ENGINE SHUTDOWN WAS THE RESULT OF THE TFI MODULE GETTING TOO HOT UNTIL I READ ABOUT THE PROBLEM IN THE NEWSPAPER. THE APPARENT CAUSE OF THE SHUTDOWNS IS THAT THE TFI MODULE IS MOUNTED TOO CLOSE TO THE ENGINE BLOCK. THE MECHANIC SHOWED ME THAT AFTER 1995 FORD MOVED THE UNIT TO UNDERNEATH THE FENDER AWAY FROM ENGINE. I READ ABOUT THE JUDGE IN CALIFORNIA WHO ORDER A RECALL OF ALL FORD VEHICLES WITH THIS PROBLEM (AUG 8, 2000) I WROTE FORD AND ASKED FOR A REFUND OF THE MONEY I SPENT REPLACING THE UNIT. I ALSO REQUESTED THAT IF REPLACING THE UNIT DID NOT SOLVE THE PROBLEM THAT FORD SHOULD MAKE THE NECESSARY MODIFICATIONS TO FIX IT
BOTH DRIVER'S SIDE AND PASSENGER'S SIDE MIRRORS FAILED AT ANY SPEED. I HAVE REPLACED THEM TWICE BECAUSE THERE WAS NO TENSION ADJUSTMENT TO PREVENT THE MIRRORS FROM BEING BLOWN BACK TO A USELESS POSITION. I KNOW OF 4 OTHER OWNERS WITH THE SAME PROBLEM. BUT JUST TRAVELING DOWN THE ROAD EVERY 1988-1989 FORD RANGER OUTFITTED WITH THE BLACK ABS PLASTIC "FLAG" STYLE MIRROR HAS THIS PROBLEM. *AK
WHILE DRIVING ON HIGHWAY ALL OF A SUDDEN THE REARVIEW MIRROR LOST TENSION AND FELL OFF. CONTACTED DEALER WHO KNEW THAT THERE WAS A PROBLEM. MIRROR WAS ATTACHED WITH TWO SCREWS. HAS BEEN REPLACED 9 TIMES. *AK
IGNITION SWITCH IS VERY WARM TO THE TOUCH AFTER OPERATION. I UNDERSTAND SOME FORDS WITH THIS SWITCH HAVE BEEN RECALLED, BUT NOT MINE. WHY? *AK
THE SHOULDER HARNESS DOES NOT RETRACT AFTER YOU LEAN FORWARD,LEAVING IT LOOSE AND USELESS AS A RESTRAINT .
VEHICLE IS NOT INCLUDED IN RECALL NOTICE (98E01000) FOR REPAIRS FOR BRAKE ROTOR FAILURE. HOWEVER, TWO RECALLS WERE DONE AND IT DOES NOT SHOW THAT IT HAS BEEN DONE. *YC
ENGINE VALVE LIFTER IS MAKING A LOUD TAPPING NOISE. DEALER HAS BEEN CONTACTED. *AK
SILICONE GASKET MATERIAL DETERIORATES AND CLOGS OIL PUMP PICKUP.
GENERAL ENGINE FAILURE OCCURS WHEN OEM OIL PAN GASKET FAILS AND PLUGS OIL PUMP PICKUP AND PRODUCES A LOW OR NO OIL PRESSURE SITUATION INTERNALLY. SB BC307291-228, 94-1-11 AND 94-6-15 RELATED TO THIS PROBLEM.
BRAKE LINES BURST TWICE IN A 2-YEAR PERIOD.BOTH COULD HAVE BEEN SERIOUS.THE PROBLEM OCCERS WHEN BRAKING HARD. *AK
DRV DOOR PWR WINDOW WON'T STAY UP\PASS SIDE PWR WINDOW WON'T GO DOWN . REAR DRV SIDE BRAKE SHOES WORN OFF {STUCK IN THE STOP POS ?} CAUSING SMOKE
Fire
DRV DOOR PWR WINDOW WON'T STAY UP\PASS SIDE PWR WINDOW WON'T GO DOWN . REAR DRV SIDE BRAKE SHOES WORN OFF {STUCK IN THE STOP POS ?} CAUSING SMOKE
Fire
HOOD LATCH STICKING ON OCCASIONS.
THE EEC-IV COMPUTER SYSTEM FAILED.
ENGINE MALFUNCTIONED, OIL KEEPS FILLING UP WITH GAS AND BLOWS GRAY SMOKE.
HOOD LATCH FAILS TO LATCH PROPERLY.
CLUTCH ROD RETAINER FELL TO THE FLOOR ON TWO OCCASIONS.
UPON STARTING RADIO/WINDSHIELD WIPER/DASH INSTRUMENTS WORKED, BUT WHEN MOTOR STARTS EVERY THING TURNS OFF, REPAIR WIRING AT IGNITION SWITCH AND REPLACED SWITCH.
VEHICLE STALLS IN TRAFFIC AT SPEEDS OF 45 MPH OR UNDER.
WHILE CONSUMER'S WIFE WAS DRIVING HOME AUTOMOBILE BEGAN TO ACT UP. AFTER DRIVING APPROX 2 MILES SHE SMELLED SMOKE, AND SHE STOPPED AND OPENED THE HOOD AND FOUND THE ENGINE ON FIRE. IT SPREAD TO THE DASH, AND BURNED THE SEATS INSIDE. *AK
Fire
METAL BAR WHICH CONNECTS THE STEERING GEAR TO TIE ROD WOR EOUT, CAUSING STEERING TO FAIL, RESULTING IN AN ACCIDENT. *AK
Crash
THE BRAKE PISTON HANGS UP AND DOES NOT RELEASE ON THE LEFT FRONT BRAKE. THE CALIPER DOES NOT RELEASE AND THE ROTORS GET EXTREMELY HOT, CAUSING DRIVER TO LOSE BRAKES. THE DEALER HAS NOT BEEN CONTACTED. *AK
THE BRAKE PISTON HANGS UP AND DOES NOT RELEASE ON THE LEFT FRONT BRAKE. THE CALIPER DOES NOT RELEASE AND THE ROTORS GET EXTREMELY HOT, CAUSING DRIVER TO LOSE BRAKES. THE DEALER HAS NOT BEEN CONTACTED. *AK
WHILE DRIVING IN HOT CONDITIONS, THE VEHICLE ENGINE SHUTS DOWN, CAUSING THE VEHICLE TO STALL. *AK
VEHICLE WAS DESTROYED DUE TO FIRE THAT STARTED IN THE DASHBOARD. *AK
Fire
WEATHER RAINING, PULLING OUT OF PARKING LOT, ANOTHER VEHICLE SWERVED IN FRONT (HYDROPLANED), WENT OFF INCLINE (SHOULDER) & HIT TREE, SHOULDER BELT FAILED TO RESTRAIN PASSENGER, WHO IN TURN HIT WINDSHIELD, HAD VEHICLE TOWED TO DEALERSHIP. *AK
Crash
1 injured
TRAILER HITCH BROKE, CAUSING ACCIDENT.(OHIO POLICE REPORT)