WHILE AT A COMPLETE STOP ON A CITY STREET BEHIND A CITY BUS WHICH WAS LOADING PASSENGERS WITH NO COLLISION OR CONTACT, THE PASSENGER SIDE AIRBAG DEPLOYED. THE AIRBAG CAUSED BURNS TO THE PASSENGER'S HAND AND BOTH KNEES. IT ALSO CAUSED DEEP CONTUSIONS ON THE LEFT KNEE, CAUSING DIFFICULTIES WITH WALKING.
1 injured
TL* THE CONTACT OWNS A 1996 BUICK LESABRE. THE VEHICLE WAS TAKEN FOR A TUNE-UP WHERE IT WAS DIAGNOSED THAT THE VALVE COVER GASKETS, UPPER INTAKE MANIFOLD, AND THE OIL PAN GASKET NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 119,000.
TL* THE CONTACT OWNS A 1996 BUICK LESABRE. WHILE DRIVING AT 40 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE FAILURE RECURRED THREE TIMES. THE CONTACT ALSO STATED THAT THE VEHICLE FAILED TO START. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATELY FAILURE MILEAGE WAS 116,000.
HAD TO REMOVE DOME LIGHT BULBS BEAUSE IT DOESNT TURN OFF, THE LIGHTS ON THE REAR ST TIMES AND I'V JUST BOUGHT A SECOND BATTERY 3 DAYS AGO BECAUSE THE LIGHTING PROBLEM CAUES THEM TO BURN OUT. SOMETIMES THE LIGHTS WILL FADE OUT. MST TIME IT DOESNT AND I CAN'T TURN THEM OFF MANUALLY EITHER. JUST FOUND OUT ABOUT THE RECALLS ON THIS VEHICLE. *TR
HAD TO REMOVE DOME LIGHT BULBS BEAUSE IT DOESNT TURN OFF, THE LIGHTS ON THE REAR ST TIMES AND I'V JUST BOUGHT A SECOND BATTERY 3 DAYS AGO BECAUSE THE LIGHTING PROBLEM CAUES THEM TO BURN OUT. SOMETIMES THE LIGHTS WILL FADE OUT. MST TIME IT DOESNT AND I CAN'T TURN THEM OFF MANUALLY EITHER. JUST FOUND OUT ABOUT THE RECALLS ON THIS VEHICLE. *TR
TL* THE CONTACT OWNS A 1996 BUICK LESABRE. THE CONTACT STATED THAT THE COURTESY LIGHTS WOULD ILLUMINATE AT ANY TIME EVEN WHEN THE VEHICLE WAS TURNED OFF. THE VEHICLE WOULD ALSO EXHIBIT A CHIMING NOISE, CAUSING THE BATTERY TO DRAIN. THE VEHICLE WAS TAKEN TO A LOCAL MECHANIC WHO WAS UNABLE TO DIAGNOSE THE FAILURE. THE MANUFACTURER WAS ALSO CONTACTED AND DENIED ANY ASSISTANCE WITH REPAIRS TO THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND CURRENT MILEAGE WAS 108,000.
TL* THE CONTACT OWNS A 1996 BUICK LESABRE. THE CONTACT STATED THAT WHILE DRIVING 20 MPH, HE HEARD A LOUD CLUNKING NOISE, THE ENGINE DROPPED, AND THE STEERING WHEEL SEIZED. THE VEHICLE WAS TOWED TO A LOCAL REPAIR SHOP, WHERE THEY DIAGNOSED THAT THE ENGINE CRADLE AND BUSHING WERE CORRODED AND NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND CURRENT MILEAGES WERE 140,000.
THE SUBFRAME RUSTED AND DROPED OUT OF THE CAR, CAUSING THE CAR TO LOSE STEERING AND SENDING IT INTO ONCOMING TRAFFIC . *TT
1. WHILE DRIVING A BUICK LESABRE ON DRY, SMOOTH, HARD-SURFACE ROAD... IN AN INSTANT... 2. ALL STEERING CONTROL WAS LOST. VEHICLE WAS BROUGHT TO A STOP WITH BRAKES. NO DEATH, NO INJURY, NO ADDITIONAL DAMAGE 3. THE ENGINE CRADLE BOLTS WERE FOUND BROKEN... THIS ALLOWED THE STEERING MECHANISM TO BECOME DISCONNECTED.... THE BOLTS WERE REPLACED, THE MECHANISM WAS CONNECTED, AND THE VEHICLE WAS RETURNED TO SERVICE 4. I CONTACTED THE PEOPLE AT BUICK 25 MAY.... AFTER FOUR DAYS OF DELAYS, THEY INFORMED ME OF THEIR DISINTEREST IN THIS CRITICAL FAILURE, REGARDLESS OF IT'S CERTAINTY TO RESULT IN FATALITIES.... PLEASE DISSEMINATE AN IMMEDIATE ALERT/RECALL/NOTICE/OTHER FYI..... YOUR FORM IS ENTITLED 'COMPLAINT'..... UNDERSTAND THIS IS AN OBJECTIVE, FACTUAL REPORT, NOT A COMPLAINT. *TR
TL* THE CONTACT OWNS A 1996 BUICK LESABRE. UPON STARTING THE VEHICLE, THE CONTACT COULD HEAR THE VEHICLE BACK FIRE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE REPAIRS WERE MADE TO STOP AN EVAPORATOR LEAK. THE REPAIR DID NOT STOP THE VEHICLE FROM BACK FIRING. THE MANUFACTURER STATED THAT BECAUSE THE VEHICLE WAS OLDER THAN 10 YEARS OF AGE, THEY COULD NOT PROVIDE ANY ASSISTANCE. THE APPROXIMATE FAILURE MILEAGE WAS 90,000 AND THE CURRENT MILEAGE WAS 98,000.
WHILE WAITING IN A PARKING LOT LANE FOR A PARKING SPACE TO OPEN, THE DRIVER'S AIRBAG DEPLOYED. I WAS NOT LEANING FORWARD, BUT I WAS LOOKING SLIGHTLY TO THE LEFT. THE BAG JUST HIT ME ON THE RIGHT SIDE FOREHEAD AND COVERED ME IN POWDER. I COULD NOT HEAR OUT OF MY RIGHT EAR, AND STILL CANNOT TODAY. *TR
1 injured
I WAS DRIVING BACK HOME FROM A FRIENDS HOUSE AND HAD THE CAR PARKED IN MY DRIVE WAY AND IT WAS LEFT RUNNING AND IT WAS IN PARK THEN I WENT OUT TO LEAVE AND THE CAR WAS RUNNING FOR ABOUT 3 MIN SITTING THERE AND I PUT IT INTO REVERSE AND IT WOULD NOT MOVE NO MATTER WHAT SO I TRIED ALL THE GEARS IT WOULDN'T WORK SO I SHUT OFF THE CAR LET IT SIT FOR ABOUT 5 MIN AND STARTED IT UP THEN PUT IT INTO REVERSE AGAIN AND IT DID THEN I DROVE ABOUT 50-100 FT AND IT FELT LIKE IT WAS SLIPPING AND THEN JUST THE OTHER DAY I WENT OUT TO START IT AND IT WAS STILL IN PARK AND IT SOUNDS LIKE A POWERSTEERING PUMP WITH NO FLUID AND IT SOUNDS LIKE A BIG NEST OF BEES AND I CHECKED THE FLUID LEVEL AND THE FLUID WAS BURNT AND THERE WAS DEBRIS IN THE FLUID SO THE CAR DON'T WORK. SO MY FAMILY HAD TO GO BUY A NEW CAR WHEN WE ARE BROKE AND NOW I HAVE NO WAY TO GET TO WORK. THERE WAS NOTHING DONE TO RESOLVE THE FAILURE YET IM GOING TO GO BUY A NEW TRANSMISSION. *TR
TL*THE CONTACT OWNS A 1996 BUICK LESABRE. WHILE DRIVING DOWN A HILL AT AN UNKNOWN SPEED, THE BRAKE INDICATOR ILLUMINATED AND MADE A CONSTANT BEEPING NOISE. THE CONTACT PARKED THE VEHICLE AND HAD AAA TOW IT TO THE DEALER. SHE PURCHASED THE VEHICLE FROM THE DEALER IN SEPTEMBER OF 2008 AND NOW SHE NEEDS NEW BRAKES. WITHIN TWO HOURS, THE VEHICLE WAS REPAIRED AT THE COST OF $400. SHE WAS VERY SKEPTICAL OF THE REPAIRS AND TOOK THE VEHICLE TO A PRIVATE MECHANIC. SHE WAS INFORMED THAT THE BRAKE LINES WERE CLOGGED. THE REPAIR WOULD COST $500. THE FAILURE MILEAGE WAS 114,000. 4/01/09 *NJ UPDATED 04/09/09.*JB
TL*THE CONTACT OWNS A 1996 BUICK LESABRE. ONE YEAR AGO, THE BRAKES FAILED TO RESPOND ON THE VEHICLE WHILE LEAVING THE DRIVEWAY. THE VEHICLE DID NOT STOP AND STRUCK ANOTHER ONE OF THE CONTACT'S VEHICLES. THERE WERE NO INJURIES. HE INSPECTED THE VEHICLE AND NOTICED THAT THE BRAKE LINE WAS SPLIT IN HALF DUE TO CORROSION. THE CONTACT REMOVED THE LINES AND INSTALLED NEW ONES. RECENTLY, THE BRAKES FAILED TO FUNCTION AGAIN. THE DRIVER STRUCK THE CURB AT 10 MPH IN ORDER TO STOP THE VEHICLE. IT WAS DISCOVERED THAT THE FRONT BRAKE LINE WAS SEVERELY CORRODED. THE VEHICLE WAS NOT TAKEN TO A MECHANIC AND THE CONTACT MADE THE REPAIRS HIMSELF. HE HAS NOT YET NOTIFIED THE MANUFACTURER. THE CURRENT MILEAGE WAS 65,000 AND FAILURE MILEAGE WAS APPROXIMATELY 60,000.
Crash
1996 BUICK LESABRE CUSTOM SUDDENLY STARTED SMOKING,OVERHEATED AND SHUT OFF ON INTERSTATE AT 60 MPH. OWNER HAD CAR TOWED AND CHECKED BY MECHANIC. CRACKED MANIFOLD LEAKING COOLANT WAS THE CAUSE, ENGINE BLOWN IS DIAGNOSIS. *TR
THE GROMMETS AND/OR WASHERS THAT HOLD UP THE ENGINE FRAME CRADLE RUSTED OUT AND ALLOWED THIS PART TO DROP THROUGH THE RETAINING BOLTS, ONCE THIS HAPPENED THERE WAS A TOTAL LOSS OF STEERING. HAD I BEEN DRIVING ON THE INTERSTATE OR 60 MPH ON A STATE HIGHWAY THIS WOULD HAVE TURNED INTO A VERY SERIOUS ACCIDENT. I WAS SITTING AT A STOPLIGHT AND THE MOMENT I ACCELERATED I HEARD A VERY LOUD METALLIC THUD/SOUND, WHICH I ASSUME WAS THE CRADLE DROPPING DOWN. I'M AMAZED THAT THIS ALL HAPPENED WITH ZERO WARNING THAT THEY WERE ANY ISSUES WITH THE STEERING. THERE WAS NEVER ANY INDICATION THAT THIS WAS GOING TO HAPPEN, MEANING NO LOOSENESS, NO VIBRATION, NO SENSORY CHANGES IN HOW THE STEERING FELT BUT ALL IN A MATTER OF 2 SECONDS, A LOUD NOISE AND THEN I COULDN'T STEER OR GUIDE THE CAR. I HIT THE BRAKES BECAUSE I WAS TRYING TO TURN RIGHT AND THE CAR WAS MOVING LEFT SO I SLAMMED ON THE BRAKES TO AVOID HITTING ONCOMING TRAFFIC. I LIVE IN THE MIDWEST AND I BELIEVE THAT THE CORROSION WAS ADVANCED DUE TO ALL THE SALT THAT IS PLACED ON THE ROADS TO MELT THE ICE/SNOW DURING THE WINTER MONTHS. I'M WRITING THIS IN HOPE THAT OTHERS WILL BE NOTIFIED AND POSSIBLY HAVE THE CONDITION OF THEIR CRADLES CHECKED OUT TO AVOID LOSING THEIR STEERING. *TR
THE GROMMETS AND/OR WASHERS THAT HOLD UP THE ENGINE FRAME CRADLE RUSTED OUT AND ALLOWED THIS PART TO DROP THROUGH THE RETAINING BOLTS, ONCE THIS HAPPENED THERE WAS A TOTAL LOSS OF STEERING. HAD I BEEN DRIVING ON THE INTERSTATE OR 60 MPH ON A STATE HIGHWAY THIS WOULD HAVE TURNED INTO A VERY SERIOUS ACCIDENT. I WAS SITTING AT A STOPLIGHT AND THE MOMENT I ACCELERATED I HEARD A VERY LOUD METALLIC THUD/SOUND, WHICH I ASSUME WAS THE CRADLE DROPPING DOWN. I'M AMAZED THAT THIS ALL HAPPENED WITH ZERO WARNING THAT THEY WERE ANY ISSUES WITH THE STEERING. THERE WAS NEVER ANY INDICATION THAT THIS WAS GOING TO HAPPEN, MEANING NO LOOSENESS, NO VIBRATION, NO SENSORY CHANGES IN HOW THE STEERING FELT BUT ALL IN A MATTER OF 2 SECONDS, A LOUD NOISE AND THEN I COULDN'T STEER OR GUIDE THE CAR. I HIT THE BRAKES BECAUSE I WAS TRYING TO TURN RIGHT AND THE CAR WAS MOVING LEFT SO I SLAMMED ON THE BRAKES TO AVOID HITTING ONCOMING TRAFFIC. I LIVE IN THE MIDWEST AND I BELIEVE THAT THE CORROSION WAS ADVANCED DUE TO ALL THE SALT THAT IS PLACED ON THE ROADS TO MELT THE ICE/SNOW DURING THE WINTER MONTHS. I'M WRITING THIS IN HOPE THAT OTHERS WILL BE NOTIFIED AND POSSIBLY HAVE THE CONDITION OF THEIR CRADLES CHECKED OUT TO AVOID LOSING THEIR STEERING. *TR
TL*THE CONTACT OWNS A 1996 BUICK LESABRE. THE HORN WOULD NOT STOP BLOWING FOR 50 MILES AFTER THE KEY WAS INSERTED INTO THE DOOR LOCK. THE DEALER STATED THAT THE FAILURE WAS ELECTRICAL AND THE REMOTE KEY NEEDED TO BE REPLACED. THE DEALER ALSO STATED THAT THE HORN WAS BLOWING WHEN THE CONTACT ARRIVED AND THEY WERE UNABLE TO REPROGRAM THE REMOTE KEY; HOWEVER, THE HORN STOPPED BLOWING. THE CONTACT REQUESTED THE OLD REMOTE KEY SINCE IT WAS UNABLE TO BE REPROGRAMMED. APPROXIMATELY ONE WEEK LATER, THE HORN BEGAN BLOWING AGAIN INTERMITTENTLY. WHILE DRIVING APPROXIMATELY 40 MPH, THE INSTRUMENT PANEL LIGHTS ILLUMINATED. THE DEALER STATED THAT THERE WAS NO VIN INFORMATION IN THEIR DATABASE. THE VIN WAS CONFIRMED WITH THE CONTACT, BUT APPEARS TO BE INVALID. THE ENGINE SIZE AND POWERTRAIN WERE UNAVAILABLE. THE FAILURE MILEAGE WAS 35,000 AND CURRENT MILEAGE WAS 83,000.
TL*THE CONTACT OWNS A 1996 BUICK LESABRE. WHILE DRIVING 25 MPH, THE CONTACT STRUCK A POTHOLE AND LOST CONTROL OF THE VEHICLE. HE NOTICED THAT THE FOUR REAR WASHERS WERE RUSTED, WHICH CAUSED THE ENGINE AND TRANSAXLE FRAME TO DETACH FROM THE VEHICLE. AS OF OCTOBER 24, 2007, THE DEALER HAD NOT INSPECTED THE VEHICLE. THE CONTACT REPLACED FOUR UPPER AND LOWER WASHERS AND ISOLATORS, IN ADDITION TO FOUR BOLTS. THE FAILURE MILEAGE WAS 70,620 AND CURRENT MILEAGE WAS 70,670. UPDATED 12/07/07
Crash
TL* - THE CONTACT HAS A 1996 BUICK LESABRE WHICH HAS A HOLE IN THE UPPER INTAKE MANIFOLD. THE GENERAL MOTORS DEALER STATED THAT THERE WAS NO RECALL ON THE VEHICLE. HE THEN CALLED THE BUICK DEALER WHO CONCERURED. THE CONTACT FOUND RECALL 96V116000 ON THE NHTSA WEBSITE. *AK
1996 BUICK LESABRE ALARM SYSTEM GOES OFF WHEN THE CAR IS TURNED ON. CONSUMER WOULD LIKE LIST OF RECALLS. *KB *JB
THERE ARE TWO RECALLS ON YOUR SITE RELATED TO MY VEHICLE. TWO DEALERS TELL ME THERE ARE NO RECALLS ON MY CAR. EVEN THOUGH THERE IS ONE CAMPAIGN STICKER LOCATED UNDER THE HOOD. I HAVE A BUICK LASABRE 1996 IT BACK FIRES WHEN STARTING. CAN YOU CHECK AND SEE IF THE TWO YOU LIST ARE ASSSOCEATED WITH MY VEHICLE. *JB
THERE ARE TWO RECALLS ON YOUR SITE RELATED TO MY VEHICLE. TWO DEALERS TELL ME THERE ARE NO RECALLS ON MY CAR. EVEN THOUGH THERE IS ONE CAMPAIGN STICKER LOCATED UNDER THE HOOD. I HAVE A BUICK LASABRE 1996 IT BACK FIRES WHEN STARTING. CAN YOU CHECK AND SEE IF THE TWO YOU LIST ARE ASSSOCEATED WITH MY VEHICLE. *JB
VEHICLE FAILED TO STOP DUE TO A LOSS OF BRAKE FLUID. INSPECTION REVEALED STEEL BRAKE TUBES SEVERELY RUSTED ONLY IN THE AREA OF THE LEAK. LEAK LOCATION IS DIRECTLY BELOW ABS HYDRAULIC CONTROL UNIT IN THE LEFT FRONT OF THE ENGINE COMPARTMENT. ALL FOUR OUTPUT LINES FROM THE ABS SYSTEM TO THE WHEEL WERE AFFECTED. THE BALANCE OF THE BRAKE LINES ON THIS VEHICLE EXHIBIT A NORMAL LEVEL OF CORROSION. *NM
DT: THE MOUNTS ON THE ENGINE CRADLE BROKE AND DROPPED AND STEERING DISENGAGED. THE RACK AND PINION FELL WITHIN THE ENGINE. OWNER WAS IN A PARKING LOT DRIVING WHEN THIS HAPPENED. THE SPEED WAS BETWEEN 5-10 MPH. THERE WERE NO PRIOR PROBLEMS WITH THE VEHICLE. THE MANUFACTURER SAID THAT THE OWNER WILL NOT BE GETTING ANY HELP RESOLVING THIS PROBLEM TODAY. THIS HAPPENED ON JULY 20, 2005. THERE WERE NO INJURIES. THE 4 REAR MOUNTS ON THE ENGINE CRADLE BROKE. THE OWNER WAS HAVING THIS REPAIRED EVENTUALLY. THE INFORMATION PROVIDED BY THE CONSUMER WAS WHAT HE THOUGHT WAS RELEVANT TO THE COMPLAINT. ALL THE INFORMATION COLLECTED IS WHAT THE OWNER OF THE VEHICLE HAS WISH TO PROVIDE. THE OWNER WAS ON THE PHONE WITH BUICK CUSTOMER SERVICE AND THEY CONTACTED THE OWNERS DEALER AND TOLD THE OWNER THAT THEY WOULD NOT SEND ANYONE TO THE OWNERS HOME TO EXAMINE THE DAMAGE. *AK
1996 BUICK LESABRE BOTH PASSENGER AND DRIVER'S SIDE FRONT AIR BAGS DEPLOYED INADVERTENTLY.*MR THE DRIVER'S AIR BAG DEPLOYED AT 11 AM WHILE DRIVING 30 MPH. ON THE SAME DAY AT 2 PM THE PASSENGER'S AIR BAG DEPLOYED WHILE DRIVING 30 MPH. THE VEHICLE WAS NOT INVOLVED IN ANY TYPE OF COLLISION NOR DID THE AIR BAG LIGHT ILLUMINATE TO INDICATE A PROBLEM. *NM
WHILE CAR WAS PARKED BUT RUNNING, CONTACT NOTICED THAT FUEL WAS LEAKING ONTO THE DRIVEWAY. THERE WERE CHILDREN IN THE VEHICLE AT THE TIME. THE VEHICLE HAS SINCE BEEN REPAIRED. THE FUEL LINE, FUEL PUMP AND FUEL SENDER WERE REPLACED. *AK
WHILE CAR WAS PARKED BUT RUNNING, CONTACT NOTICED THAT FUEL WAS LEAKING ONTO THE DRIVEWAY. THERE WERE CHILDREN IN THE VEHICLE AT THE TIME. THE VEHICLE HAS SINCE BEEN REPAIRED. THE FUEL LINE, FUEL PUMP AND FUEL SENDER WERE REPLACED. *AK
WHILE CAR WAS PARKED BUT RUNNING, CONTACT NOTICED THAT FUEL WAS LEAKING ONTO THE DRIVEWAY. THERE WERE CHILDREN IN THE VEHICLE AT THE TIME. THE VEHICLE HAS SINCE BEEN REPAIRED. THE FUEL LINE, FUEL PUMP AND FUEL SENDER WERE REPLACED. *AK
VEHICLE COMMENCED TO ACCELERATE FROM A STOP POSITION WHILE THE BRAKES WERE APPLIED. VEHICLE TOOK OFF FROM 0-45 MPH. CONSUMER RODE THE BRAKES, AND DOWN SHIFTED THE TRANSMISSION TO GAIN CONTROL. DEALER WAS NOT NOTIFIED.*AK
A LOUD CLANKING NOISE WAS COMING FROM THE FRONT WHILE DRIVING, VEHICLE STALLED. CONSUMER WAS UNABLE TO RESTART VEHICLE, AND HAD IT TOWED TO THE DEALER. MECHANIC DETERMINED THAT THE WARPED INTAKE MANIFOLD NEEDED TO BE REPLACED. *AK
WHEN PARKING BOLTS SHREDDED OFF THE FRONT RACK AND PINION. DEALERSHIP WAS NOTIFIED, BUT DID NOT RESOLVE THE PROBLEM. *AK
WHILE DRIVING 30 MPH PASSENGER'S SIDE AIR BAG DEPLOYED INADVERTENTLY. *AK
NAR 9-8-03. MINOR KNOCK NOISE IN ENGINE. ENGINE WAS REPLACED IN THE AMOUNT OF $4200.00 ON 71000 MILE VEHICLE. *CB
MY 1996 BUICK LESABRE ABS WARNING LIGHT DID NOT LET ME KNOW THAT THE ABS WERE NOT WORKING, RESULTING IN AN ACCIDENT.*AK
Crash
THE UPPER MANIFOLD HAD DETERIORATED OR CRACKED ALLOWING COOLANT FLUID TO ENTER THE COMBUSTION CHAMBER. VEHICLE'S ENGINE SEIZED. *PH *MR
ENGINE STOPPED UNEXPECTEDLY AND SUDDENLY AT 25 MPH. VEHICLE HAD TO BE TOWED TO THE DEALER. THE DEALER STATED THE PROBLEM WAS A CRACKED MANIFOLD. *AK
CONSUMER TOOK VEHICLE TO DEALER FOR INSPECTION, AND MECHANIC NOTICED THAT THE PLASTIC INTAKE MANIFOLD CRACKED, CAUSING FLUID TO LEAK ONTO THE ENGINE.*AK
CONSUMER STATES VEHICLE GOT OVERHEATED AND COOLANT WENT INSIDE THE ENGINE DUE TO PLASTIC INTAKE MANIFOLD. DEALER CHANGED TWICE THE INTAKE MANIFOLD. *AK
ENGINE SUSTAINED DAMAGE DUE TO OIL SLUDGING (GELLING). OIL PRESSURE WAS INFLATED,KNOCKING SOUND WAS NOTICED. PENZOIL 10W30 WAS BEING USED AT REGULAR INTERVALS. DIMSII IVOQ ENTRY POSTED AFTER 12/12/02 CUT-OVER TO ARTEMIS----770781. *AK *NLM
WHILE TRAVELING ON THE HIGHWAY AND WITHOUT PRIOR WARNING, THERE WAS ANTIFREEZE LEAKING FROM UNDERNEATH THE MANIFOLD, THE DEALER HAD BEEN NOTIFIED, PLEASE PROVIDE ADDITIONAL INFORMATION.*JB
THE UPPER MANIFOLD CRACKED AND LEAKED ANTIFREEZE.TS *JB
CONSUMER NOTICED ANITFREEZE ON THE DRIVEWAY UNDER THEIR VEHICLE. THE CONSUMER TOOK VEHICLE TO THE DEALERSHIP TO HAVE IT SERVICED. THE DEALERSHIP INDICATED THAT THERE WAS A CRACK IN THE UPPER MANIFOLD, WHICH WAS THE CAUSE OF THE LEAK. THERE'S A SERVICE BULLETIN FOR THIS PART, THE EGR VALVE WAS REPLACED BECAUSE OF EXCESSIVE HEAT. THE CONSUMER REQUESTED REIMBURSEMENT FOR REPAIRS. *TS *JG *NLM
CONSUMER STATED WHILE DRIVING AT SLOW SPEED, THE FUEL PUMP FAILED. DEALER NOTIFIED. TS *TT
WHILE DRIVING AND WITH NO WARNING COURTESY LIGHTS INSIDE VEHICLE WILL FLICKER ON AND OFF, CAUSING CONSUMER TO HAVE VISUAL PROBLEMS WHILE DRIVING. DEALER NOTIFIED.*AK
CONSUMER STATES BATTERY EXPLODED, AND REQUESTING ASSISTANCE FROM MANUFACTURER.*JB
CONSUMER STATES BATTERY EXPLODED, AND REQUESTING ASSISTANCE FROM MANUFACTURER.*JB
ANOTHER VEHICLE CUT IN FRONT. CONSUMER APPLIED BRAKES BUT HIT OTHER VEHICLE ON RIGHT FRONT. UPON IMPACT WITH OTHER VEHICLE, AIR BAGS DEPLOYED. DRIVER WAS JAMMED IN SEAT, AND UNABLE TO GET OUT. VEHICLE FILLED WITH SMOKE AN POWDER SUBSTANCE WHICH CAUSED DRIVER'S EYES AND THROAT TO BE IRRITATED.*AK
Crash
ANOTHER VEHICLE CUT IN FRONT. CONSUMER APPLIED BRAKES BUT HIT OTHER VEHICLE ON RIGHT FRONT. UPON IMPACT WITH OTHER VEHICLE, AIR BAGS DEPLOYED. DRIVER WAS JAMMED IN SEAT, AND UNABLE TO GET OUT. VEHICLE FILLED WITH SMOKE AN POWDER SUBSTANCE WHICH CAUSED DRIVER'S EYES AND THROAT TO BE IRRITATED.*AK
Crash
WINDSHIELD HAS CRACKED THREE TIMES UNDER NORMAL DRIVING CONDITIONS, AND HAS BEEN REPLACED ON EACH OCCASION. *AK