Complaint Statistics
85 total complaints
7 crashes 6 fires 12 injuries
Top Reported Components
| Component | Complaints |
| SERVICE BRAKES, HYDRAULIC:ANTILOCK/TRACTION CONTROL/ELECTRONIC LIMITED SLIP | 7 |
| ENGINE AND ENGINE COOLING | 5 |
| ENGINE AND ENGINE COOLING:ENGINE | 5 |
| AIR BAGS:FRONTAL | 4 |
| ENGINE AND ENGINE COOLING:ENGINE:GASOLINE | 4 |
| SERVICE BRAKES, HYDRAULIC:FOUNDATION COMPONENTS:HOSES, LINES/PIPING, AND FITTINGS | 4 |
| SERVICE BRAKES, HYDRAULIC:FOUNDATION COMPONENTS | 4 |
| EQUIPMENT:APPLIANCE:AIR CONDITIONER | 3 |
| SUSPENSION:FRONT | 3 |
| ELECTRICAL SYSTEM | 3 |
Incident date: May 31, 2014
ON 5/31/14, MY 1997 MITSUBISHI MONTERO WAS PARKED IN MY DRIVEWAY. WHEN I WENT TO GET INTO THE VEHICLE, I NOTICED A LARGE BURN IN THE BACK OF THE DRIVER'S SIDE SEAT. AFTER CALLING MITSUBISHI, THE FIRE DEPARTMENT CAME SINCE IT WAS STILL SMOLDERING AND DISCONNECTED THE BATTERY. THEY BELIEVED IT TO BE A
... N ELECTRICAL SHORT. AFTER MANY FOLLOW-UP CALLS TO MITSUBISHI, THEY BELIEVE IT WAS CAUSED BY WEAR AND TEAR SINCE THE CAR WAS 17 YEARS OLD. ALL OF THE COST TO FIX THE ISSUE WAS ON ME AS THE OWNER. *TRRead more
Fire
Incident date: May 31, 2014
ON 5/31/14, MY 1997 MITSUBISHI MONTERO WAS PARKED IN MY DRIVEWAY. WHEN I WENT TO GET INTO THE VEHICLE, I NOTICED A LARGE BURN IN THE BACK OF THE DRIVER'S SIDE SEAT. AFTER CALLING MITSUBISHI, THE FIRE DEPARTMENT CAME SINCE IT WAS STILL SMOLDERING AND DISCONNECTED THE BATTERY. THEY BELIEVED IT TO BE A
... N ELECTRICAL SHORT. AFTER MANY FOLLOW-UP CALLS TO MITSUBISHI, THEY BELIEVE IT WAS CAUSED BY WEAR AND TEAR SINCE THE CAR WAS 17 YEARS OLD. ALL OF THE COST TO FIX THE ISSUE WAS ON ME AS THE OWNER. *TRRead more
Fire
Incident date: Apr 16, 2011
1997 MITSUBISH MONTERO 3.5 LITER AUTOMATIC- CRANK SHAFT BOLT HAS COME OUT ON 5 SEPARATE OCCASIONS AND HAS COST OVER $3000 TO HAVE IT REPLACED. THE INSIDE OF THE CRANKSHAFT WHERE THE BOLT GOES IS COMPLETELY STRIPPED TO THE POINT I NOW HAVE TO REPLACE THE ENGINE. THIS IS NOT AN ISOLATED ISSUE AS THI
... S APPEARS TO BE AN INHERENT PROBLEM WITH ALL YEARS OF MONTEROS. THERE SHOULD BE A RECALL FOR THIS AND MITSUBISHI SHOULD COVER THE COST FOR THERE NEGLIGENCE. *TRRead more
Incident date: May 12, 2009
CRANKSHAFT PULLEY PIN/BOLT GETS SHEARED OFF. DASH LIGHTS COME ON AND VEHICLE POWER STEERING STOPS WORKING AS THE PUMP IS NOT TURNING BECAUSE THE PROBLEM AFFECT THE ENTIRE PULLEY SYSTEM. IT ALSO AFFECTS THE TIMING GEAR/BELT/HARMONIC BALANCER. THIS IS THE 3RD TIME IN AS MANY YEARS THIS HAS HAPPENED. T
... HIS IS THE 2ND MECHANIC WHO HAS TOLD ME THAT IT'S AN ENGINE DEFECT BECAUSE THE PIN/BOLT IS TOO SHORT. THERE IS NO WARNING BEFORE IT HAPPENS. IT OCCURS UNDER NORMAL CITY DRIVING CONDITIONS AT LOW OR NO SPEED. *TRRead more
Incident date: Jul 15, 2008
THE VEHICLE WAS PARKED AND IDLING. I WAS IN THE DRIVER'S SEAT WHEN A FIRE BROKE OUT AND THE FLAMES CAUSED ME SEVERE BURNS TO MY BODY. I WAS NEARLY ASPHYXIATED. THE CAR WAS A TOTAL LOSS. *TR
Fire
1 injured
Incident date: Jul 15, 2008
THE VEHICLE WAS PARKED AND IDLING. I WAS IN THE DRIVER'S SEAT WHEN A FIRE BROKE OUT AND THE FLAMES CAUSED ME SEVERE BURNS TO MY BODY. I WAS NEARLY ASPHYXIATED. THE CAR WAS A TOTAL LOSS. *TR
Fire
1 injured
Incident date: Mar 5, 2008
1997 MITSUBISHI MONTERO CRANKSHAFT PULLEY CAME LOOSE THREE TIMES WHICH CREATED NO POWER STEERING AND NO CHARGING OF THE BATTERY PURCHASED NEW CRANKSHAFT PULLEY BUT DID NOT HELP THE THIRD TIME INSTALLED A LOCK WASHER ON THE BOLT AND RE TORQUED TO SPEC LAST WEEK. *TR
Incident date: Jun 15, 2008
TL*THE CONTACT OWNS A 1997 MITSUBISHI MONTERO. WHEN THE VEHICLE WAS STARTED, THE CRANKSHAFT PULLEY DETACHED FROM THE VEHICLE. THE DEALER STATED THAT THE CONTACT WOULD BE RESPONSIBLE FOR THE REPAIR. THE VEHICLE HAS NOT BEEN DRIVEN SINCE. THE FAILURE MILEAGE WAS 190,000.
Incident date: Jun 25, 2007
STARTED CAR, NOTICED 3 RANDOM LIGHTS ILLUMINATED ON INSTRUMENT CLUSTER. THEN POWER STEERING WAS INTERMITTENT. THEN A/C WENT OUT AND WOULD NOT COOL DOWN. THEN POWER STEERING FAILED COMPLETELY. CAR WAS DRIVEN TO REPAIR SHOP NEARBY, SINCE NO LOCAL MITSUBISHI DEALER. MECHANIC FOUND CRANKSHAFT BOLT BR
... OKEN THAT LED TO POWER STEERING AND A/C PULLEY NOT WORKING. INCIDENT LED TO NEAR LOSS OF CONTROL DURING TURNING , AS POWER STEERING WOULD "KICK" IN AT TIMES DURING CORNERING AND LEAD TO OVERSTEER. HAD TO CHANGE CRANKSHAFT BOLT, HARMONIC BALANCER, TIMING BELT GEAR, AND SOMETHING ELSE. *TRRead more
Incident date: Jun 25, 2007
STARTED CAR, NOTICED 3 RANDOM LIGHTS ILLUMINATED ON INSTRUMENT CLUSTER. THEN POWER STEERING WAS INTERMITTENT. THEN A/C WENT OUT AND WOULD NOT COOL DOWN. THEN POWER STEERING FAILED COMPLETELY. CAR WAS DRIVEN TO REPAIR SHOP NEARBY, SINCE NO LOCAL MITSUBISHI DEALER. MECHANIC FOUND CRANKSHAFT BOLT BR
... OKEN THAT LED TO POWER STEERING AND A/C PULLEY NOT WORKING. INCIDENT LED TO NEAR LOSS OF CONTROL DURING TURNING , AS POWER STEERING WOULD "KICK" IN AT TIMES DURING CORNERING AND LEAD TO OVERSTEER. HAD TO CHANGE CRANKSHAFT BOLT, HARMONIC BALANCER, TIMING BELT GEAR, AND SOMETHING ELSE. *TRRead more
Incident date: Sep 26, 2005
DT*: THE CONTACT STATED THE CRANKSHAFT PULLEY AND BOLT BECAME DISCONNECTED. THIS OCCURRED TWICE.
Incident date: Sep 1, 2004
1. BRAKE LIGHT CAME ON AND HAS STAYED ON FOR A COUPLE OF DAYS. CAR WAS CHECKED OUT AND ESTIMATED CHARGES FOR REPAIRS TO FRONT BRAKE, INCLUDING NEW ROTOR, WOULD BE $1000. I WAS NOT AWARE OF THE RECALL FOR 1997 MONTEROS IN REGARD TO BRAKE LINES. *AK 2. SERVICE ENGINE SOON COMES ON AT RANDOM AND
... ONLY GOES OFF WHEN THE BATTERY IS UNHOOKED AND REHOOKED OR REPLACED.Read more
Incident date: Sep 1, 2004
1. BRAKE LIGHT CAME ON AND HAS STAYED ON FOR A COUPLE OF DAYS. CAR WAS CHECKED OUT AND ESTIMATED CHARGES FOR REPAIRS TO FRONT BRAKE, INCLUDING NEW ROTOR, WOULD BE $1000. I WAS NOT AWARE OF THE RECALL FOR 1997 MONTEROS IN REGARD TO BRAKE LINES. *AK 2. SERVICE ENGINE SOON COMES ON AT RANDOM AND
... ONLY GOES OFF WHEN THE BATTERY IS UNHOOKED AND REHOOKED OR REPLACED.Read more
Incident date: Jan 6, 2004
1 - THIS JUST STARTED HAPPENING, NO ACCIDENT OR MISUSE. 2 - VEHICLE WILL NOT START AT TIMES AND MUST KEEP TURNING IGNITION, EVENTUALLY IT STATS. (CHANGED BATTERY, TERMINALS, WIRES, ETC, WITH NO AFFECT) ALARM GOES OFF SPORADICALLY OR SETS ON IT'S OWN. DOOR LOCKS UNLOCK, THEN IMMEDIATELY LOCK BA
... CK. WINDOWS ARE NOT GOING UP CORRECTLY AND ARE TILTING SLIGHTLY CAUSING A SMALL AIR LEAK ON BOTH FRONT WINDOWS. ALL PROBLEMS ARE ANNOYING BUT I CAN STILL GET FROM POINT A TO POINT B. THIS HAPPENS EVERY DAY.*AKRead more
Incident date: Jan 6, 2004
1 - THIS JUST STARTED HAPPENING, NO ACCIDENT OR MISUSE. 2 - VEHICLE WILL NOT START AT TIMES AND MUST KEEP TURNING IGNITION, EVENTUALLY IT STATS. (CHANGED BATTERY, TERMINALS, WIRES, ETC, WITH NO AFFECT) ALARM GOES OFF SPORADICALLY OR SETS ON IT'S OWN. DOOR LOCKS UNLOCK, THEN IMMEDIATELY LOCK BA
... CK. WINDOWS ARE NOT GOING UP CORRECTLY AND ARE TILTING SLIGHTLY CAUSING A SMALL AIR LEAK ON BOTH FRONT WINDOWS. ALL PROBLEMS ARE ANNOYING BUT I CAN STILL GET FROM POINT A TO POINT B. THIS HAPPENS EVERY DAY.*AKRead more
Incident date: Jan 6, 2004
1 - THIS JUST STARTED HAPPENING, NO ACCIDENT OR MISUSE. 2 - VEHICLE WILL NOT START AT TIMES AND MUST KEEP TURNING IGNITION, EVENTUALLY IT STATS. (CHANGED BATTERY, TERMINALS, WIRES, ETC, WITH NO AFFECT) ALARM GOES OFF SPORADICALLY OR SETS ON IT'S OWN. DOOR LOCKS UNLOCK, THEN IMMEDIATELY LOCK BA
... CK. WINDOWS ARE NOT GOING UP CORRECTLY AND ARE TILTING SLIGHTLY CAUSING A SMALL AIR LEAK ON BOTH FRONT WINDOWS. ALL PROBLEMS ARE ANNOYING BUT I CAN STILL GET FROM POINT A TO POINT B. THIS HAPPENS EVERY DAY.*AKRead more
Incident date: Jul 14, 2004
WHILE DRIVING A LOUD CLANKING NOISE WAS HEARD FROM THE FRONT. ALL ELECTRICAL LIGHTS FLASHED ON THE DASHBOARD. STEERING COLUMN FAILED TO MOVE. CONSUMER WAS ABLE TO MAINTAIN THE CONTROL OF THE VEHICLE, AND DROVE IT TO THE DEALER FOR INSPECTION. MECHANIC DETERMINED THAT THE MAIN BOLT TO THE PULLEY
... BELT SHEARED OFF. *AKRead more
Incident date: Jul 8, 2004
IN EARLY 2003 I PURCHASED A 1997 MITSUBISHI MONTERO FULL SUV. IN APRIL 2003 MY GIRL FRIEND WAS DRIVING THE CAR ONE DAY , WHEN IT JUST BROKE DOWN ON HER .HEN SHE TURNED THE KEY TO START THE CAR YOU COULD HEAR THE ENGINE, BUT THE CAR WOULD NOT START.I GOT IT TOWED,AND MY MECHANIC LOOKED AT IT AN
... D SAID ONE OF THE MAIN FUSE (MFI-MULTI FUEL INJECTION) HAD BLOWN.*AK HE REPLACED THE FUSE AND THE CAR WAS FINE, TWO WEEKS LATER IT HAPPENED AGAIN , SO HE REPLACED THE FUSE AND I TOOK IT TO THE DEALER. THE DEALER CHECKED FOR ANY RECALL THERE WAS NONE.ON 7/8/04 IT HAPPENED AGAIN, BUT THIS TIME WHEN THE FUSE WAS REPLACED I TURNED OVER THE ENGINE AND THE WHOLE CAR WAS SMOKING THROUGH THE HOOD AND INSIDE THE VEHICLE I WAS SO SCARED I RAN AWAY FROM IT UNTIL THE SMOKE WENT AWAY.THE CAR WAS TOWED TO MY HOME AND MY MECHANIC SHOWED ME ALL THE BURNED WIRE IN THE HARNESS, PLEASE LET ME NOW IF THERE IS A RECALL ON THIS PROBLEMRead more
Fire
CRANKSHAFT BOLT IS LOOSENING ON VEHICLE CAUSING LOSS OF POWER STEERING.*MR CONSUMER'S VEHICLE WASN'T RECOGNIZED TO BE WITHIN THE RECALL. CONSUMER EXPERIENCED THE DEFECT AND HAD TO PAY $1355.56 FOR REPAIRS AND $130.00 FOR TOWING. CONSUMER FEELS MITSUBISHI SHOULD COVER COSTS OF REPAIRS AND TOWING DUE
... TO THE RECALL THAT WAS CREATED TO TAKE CARE OF THIS EXACT PROBLEM. *PHRead more
Incident date: Sep 1, 2003
WHILE SITTING IN TRAFFIC, PASSENGER (WIFE) MOVED HER WINDOW VISOR, A FLAME SHOT OUT TOWARDS HER FACE COMING FROM UPPER RIGHT CORNER OF WINDOW VISOR, WHERE WIRE FOR VANITY MIRROR HAD CHAFFED OVER TIME, DUE TO A PLASTIC COVERING EDGE TO HIDE WIRE.*AK FLAME WAS 4-5 INCHES LONG, 1 INCH THICK AND FLAMED
... FOR 6-8 SECONDS, THEN LARGE AMOUNTS OF THICK GREY SMOKE CAME FROM AREA. WIRE FOR VANITY MIRROR HAD CHAFFED AWAY THE WIRING COVER AND WAS TOUCHING THE METAL ROD USED TO HOLD UP VISOR. FUSE DID NOT BLOW. THIS COULD HAVE EASILY CAUGHT FIRE INSIDE MY HEADLINER, BEHIND DASH, ETC.Read more
Fire
Incident date: Aug 11, 2003
CONSUMER'S VEHICLE HAD THE SAME PROBLEM AS STATED IN RECALL 00V311002 . THE DEALER WOULD NOT REPAIR THE VEHICLE BECAUSE THE VEHICLE IDENTIFICATION NUMBER WAS NOT INCLUDED. *AK THE CRANKSHAFT BOLT LOOSENED WHICH RESULTED IN A LOST OF POWER STEERING. *TS *PH *NLM
Incident date: May 25, 2003
WHILE DRIVING AT LOW SPEED AND WITHOUT WARNING THE VEHICLE SHUT OFF. *TT
Incident date: Dec 27, 2002
PROBLEM WITH FRONT AND REAR DIFFERENTIAL REPORTED TO DEALERSHIP. THEY DID NOTHING TO FIX, JUST RESET CHECK ENGINE LIGHT. 3 WEEKS LATER CAR WAS IN A ROLLOVER ACCIDENT. DRIVER STEERED SLIGHTLY TO AVOID COLLISION WITH ANOTHER VEHICLE THAT WAS MAKING AN ILLEGAL LANE CHANGE AND MONTERO WENT OUT OF CONTRO
... L. NEITHER STEERING NOR BRAKING COULD STOP OR AFFECT WHAT WAS HAPPENING.Read more
Crash
4 injured
Incident date: Feb 1, 2002
WHILE DRIVING VEHICLE WAS LOOSING POWER. CONSUMER STATES' NOW VEHICLE WILL NOT START. TOOK TO DEALER AND THEY REPLACED THE COMPUTER, PROBLEM HAS REOCCURED. PLEASE PROVIDE ANY FURTHER INFORMATION. TS
Incident date: Nov 19, 2002
AFTER VEHICLE CRANK SHAFT PULLEY WAS IMPACTED AND DEALERSHIP INDICATED THAT IT WAS OKAY. WHILE DRIVING THE CRANK SHAFT PULLEY BROKE. THE DEALERSHIP IS REFUSING TO FIX THE VEHICLE. PLEASE PROVIDE MORE DETAILS TS
AFTER DRIVING THE CAR FOR 49 DAYS THE OIL PLUG CAME OUT, ALL THE OIL FELLOUT OF THE CAR AND ENGINE LOCKED, DEALER SAYS IT IS NOT COVERED MY WARRANTY*AK
Incident date: Jun 14, 2002
FAILURE CAUSED ERRATIC OPERATION OF POWER DOOR LOCKS, ALARM AND ALL OTHER ELECTRONIC COMPONENTS. OF SPECIAL CONCERN WAS THE RAPID FAILURE OF DOOR LOCKING COMPONENTS.
Incident date: Jun 14, 2002
FAILURE CAUSED ERRATIC OPERATION OF POWER DOOR LOCKS, ALARM AND ALL OTHER ELECTRONIC COMPONENTS. OF SPECIAL CONCERN WAS THE RAPID FAILURE OF DOOR LOCKING COMPONENTS.
Incident date: Apr 20, 2001
WHILE DRIVING ABOUT 35 MPH HIT AN ELK, AND AIR BAGS DID NOT DEPLOY. *AK
Crash
Incident date: Dec 8, 2000
VEHICLE WAS IN 40 MPH CAR COLLISION, CRASHED INTO A TREE, AND ROOF COLLAPSED. ONTO CONSUMER'S HUSBAND. HAS NOT CONTACTED DEALER YET. *AK
Crash
REAR AXLE LEAF SPRING BROKE. DEALER HAS BEEN CONTACTED.*AK
Incident date: Jan 22, 2001
BRAKE PEDAL GOES TO FLOOR. REGULAR BRAKES WOULD FAIL TO WORK WHENEVER PEDAL IS DEPRESSED. TOOK TO MECHANIC, AND HAD MASTER CYLINDER REPLACED, AND BRAKES BLED. PROBLEM STILL EXISTS. *AK
Incident date: Jan 22, 2001
BRAKE PEDAL GOES TO FLOOR. REGULAR BRAKES WOULD FAIL TO WORK WHENEVER PEDAL IS DEPRESSED. TOOK TO MECHANIC, AND HAD MASTER CYLINDER REPLACED, AND BRAKES BLED. PROBLEM STILL EXISTS. *AK
Incident date: Feb 16, 2001
ENGINE LIGHT STAYS ILLUMINATED AND NEVER GOES OFF, ON ONE OCCASION WHEN THE BATTERY WAS FAILED, THE LIGHT WENT OFF. *SLC
Incident date: Feb 16, 2001
ENGINE LIGHT STAYS ILLUMINATED AND NEVER GOES OFF, ON ONE OCCASION WHEN THE BATTERY WAS FAILED, THE LIGHT WENT OFF. *SLC
Incident date: Jul 5, 2000
THIS CAR WAS IN A MAJOR ACCIDENT & SOLD TO ME WITHOUT A MV-103 FORM OR TITLE STATING THAT THIS A REBUILT SALVAGE. NO SAFTCY DEFECT MENTIONE DIN SUMMARY. *AK
Incident date: Jul 5, 2000
THIS CAR WAS IN A MAJOR ACCIDENT & SOLD TO ME WITHOUT A MV-103 FORM OR TITLE STATING THAT THIS A REBUILT SALVAGE. NO SAFTCY DEFECT MENTIONE DIN SUMMARY. *AK
DESIGN OF THE CUP HOLDER DOES NOT HOLD A CUP PROPERLY. THIS ALLOWS THE CUP TO FALL OVER WHICH DISTRACTS THE DRIVER. ALSO, CAUSES LIQUID TO SPILL ALL OVER THE DASH, WHICH CAUSES ELECTRICAL PROBLEMS. PLEASE PROVIDE ANY FURTHER INFORMATION. *AK
Incident date: Aug 15, 1997
I HAVE NOTHING BUT PROBLEMS WITH THE BRAKES AND CD CHANGER ON THIS VEHICLE, AS WELL AS NUMBROUS OTHER PROBLEMS. PLEASE ADVISE IF I HAVE ANY RECOURSE? *AK
Incident date: Aug 15, 1997
I HAVE NOTHING BUT PROBLEMS WITH THE BRAKES AND CD CHANGER ON THIS VEHICLE, AS WELL AS NUMBROUS OTHER PROBLEMS. PLEASE ADVISE IF I HAVE ANY RECOURSE? *AK
Incident date: Nov 4, 1999
I'VE HAD SAME PROBLEMS WITH MY BRAKES TWICE NOW. MY BRAKES PULSATE AT HIGHER SPEEDS. I'VE HAD MY ROTORS RESURFACED TWICE.(1) AT 34,000 MILES & (2) AT 58840. THE WARRANTY THE DEALER SHIP GIVES ME IS 3 MONTH OR 3000 MILES FOR PULSATING, EVEN IF I WERE TO BUY NEW ROTORS. I' VE HAD TO RECENTLY REPLACE M
... Y RIGHT BACK SHOE BECAUSE IT WAS RUBBUING METAL ON METAL BUT MY LEFT SIDE WAS PERFECTLY FINE. THEY COULD'NT GIVE ME AN EXPLANATION WHY. I'M TIRED OF PAYING $ 500 FOR THE SAME PROBLEM YEAR AFTER YEAR. MY ANTENNA WAS REPLACED BECAUSE IT BROKE OFF, SO I HAD THE DEALER PUT A NEW ONE IN A YEAR AGO AND NOW THE ANTENNA DOESN'T GO DOWN. MY MOONROOFS COVER (INTERIOR ) POPPED OFF WHILE DRIVING. I SOMEHOW MANAGED TO PUT IT BACK IN. THESE ARE THE COUPLE OF PROBLEMS I'VE ENCOUNTERED. I ESPECIALLY DON'T FEEL SAFE DRIVING THIS TRUCK WHEN IT STARTS TO PULSATE. I HAVE A 4 MONTH OLD BABY & I'M ALWAYS AFRAID SOMETHING IS GOING TO GO WRONG.Read more
WHILE DRIVING 45MPH OR FASTER THE FRONT END BEGINS TO VIBRATE VERY HARD. DEALER HAS NOT BEEN CONTACTED. *AK
Incident date: Mar 1, 1999
MY SUV ON NUMEROUS OCCASIONS HAS STALLED WHEN VEHICLE COMES TO STOP. ON ONE OCCASION, MY WIFE WAS ACCELERATING FROM A STANDSTILL-WHEN THE VEHICLE STALLED. ON EACH OCCASION, WE WERE ABLE TO RESTART THE VEHICLE WITHOUT PROBLEMS. HOWEVER, WITH THE VEHICLE STALLING UPON ACCELERATING FROM STANDSTILL I
... N THE MIDDLE OF AN INTERSECTION COULD PROVE TO BE VERY DANGEROUL!!!!!!!!!!!Read more
Incident date: Sep 17, 1998
VEHICLE LOST CONTROL IN THE FRONT SUSPENSION AREA WHILE DRIVING RESULTING IN VEHICLE COLLISION, NO DEPLOYMENT OF AIR BAGS DURING IMPACT. MJS (ATTORNEY FOR CONSUMER).
Crash
2 injured
Incident date: Sep 17, 1998
VEHICLE LOST CONTROL IN THE FRONT SUSPENSION AREA WHILE DRIVING RESULTING IN VEHICLE COLLISION, NO DEPLOYMENT OF AIR BAGS DURING IMPACT. MJS (ATTORNEY FOR CONSUMER).
Crash
2 injured
Incident date: Jul 1, 1999
I AM SCARED. AT 50-70MPH THE VIBRATION FROM THE FRONT TIRES UP THROUGH THE STEERING WHEEL IS DANGEROUS, BORDERS ON LOSING CONTROL. RESEARCH ON INTERNET: THIS IS A HIGHLY COMMON PROBLEM FOR MONTERO SPORT OWNERS. PLEASE ADVISE. *AK( DOT NUMBER: )
Incident date: Jul 3, 1999
SEAT BELT ANCHOR AND ATTACHMENT BOLT SEPARATED FROM THE VEHICLE. THE DEALER HAS BEEN NOTIFIED. *AK
Incident date: Jun 3, 1999
ENTIRE FAN AND CLUTCH ASSEMBLY. SHEARED OFF WHILE I WAS TRAVELING IN INTER CITY TRAFFIC, IF THIS FAILURE WOULD HAVE OCCURRED WHILE TRAVELING ON A HIGHWAY THIS ASSEMBLY COULD HAVE DAMAGED EITHER THE STEERING, FUEL OR ELECTRICAL SYSTEM. THE LOCAL DEALER AND FACTORY REPRESENTATIVES HAVE REVIEWED AND C
... OME TO THE CONCLUSION THAT THIS IS JUST A FAILURE DUE TO MILEAGE. IF THIS IS THE CASE THERE POTENTIALLY ARE MANY VEHICLES OF THIS TYPE THAT MAY EXPERIENCE THE SAME FAILURE. *AKRead more
Incident date: Jun 3, 1999
ENTIRE FAN AND CLUTCH ASSEMBLY. SHEARED OFF WHILE I WAS TRAVELING IN INTER CITY TRAFFIC, IF THIS FAILURE WOULD HAVE OCCURRED WHILE TRAVELING ON A HIGHWAY THIS ASSEMBLY COULD HAVE DAMAGED EITHER THE STEERING, FUEL OR ELECTRICAL SYSTEM. THE LOCAL DEALER AND FACTORY REPRESENTATIVES HAVE REVIEWED AND C
... OME TO THE CONCLUSION THAT THIS IS JUST A FAILURE DUE TO MILEAGE. IF THIS IS THE CASE THERE POTENTIALLY ARE MANY VEHICLES OF THIS TYPE THAT MAY EXPERIENCE THE SAME FAILURE. *AKRead more
Showing 50 of 85 complaints.