Complaint Statistics
189 total complaints
12 crashes 6 fires 13 injuries
Top Reported Components
| Component | Complaints |
| POWER TRAIN:AUTOMATIC TRANSMISSION | 9 |
| AIR BAGS:FRONTAL | 8 |
| SERVICE BRAKES, HYDRAULIC:FOUNDATION COMPONENTS:DISC:ROTOR | 8 |
| ENGINE AND ENGINE COOLING:ENGINE | 8 |
| FUEL SYSTEM, GASOLINE:FUEL INJECTION SYSTEM | 7 |
| SERVICE BRAKES, HYDRAULIC:ANTILOCK/TRACTION CONTROL/ELECTRONIC LIMITED SLIP | 7 |
| ENGINE AND ENGINE COOLING | 6 |
| ENGINE AND ENGINE COOLING:COOLING SYSTEM | 5 |
| VISIBILITY:WINDSHIELD | 5 |
| EQUIPMENT:APPLIANCE:AIR CONDITIONER | 5 |
Incident date: Feb 13, 2013
TL* THE CONTACT OWNS A 1997 CHRYSLER CONCORDE. THE CONTACT STATED THAT THE SEAT BELT FAILED TO RETRACT. THE VEHICLE WAS NOT TAKEN TO A DEALER FOR DIAGNOSTIC TESTING. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 100,000 AND THE
... CURRENT MILEAGE WAS 125,000. .... UPDATED 10-17-13 *BF UPDATED 10/24/14*CNRead more
Incident date: Jun 30, 2008
TL* THE CONTACT OWNS A 1997 CHRYSLER CONCORDE. THE CONTACT STATED THE VEHICLE WAS INCLUDED IN THE RECALL UNDER NHTSA CAMPAIGN ID NUMBER: 98V184000 (FUEL SYSTEM, GASOLINE:FUEL INJECTION SYSTEM) AND THE VEHICLE WAS REPAIRED. EIGHT YEARS AFTER THE VEHICLE WAS REPAIRED SHE NOTICED FUEL LEAKING FROM THE
... VEHICLE WHILE IT WAS PARKED. THE CONTACT STATED FUEL WOULD ALSO LEAK WHILE DRIVING. THE VEHICLE WAS TAKEN AN INDEPENDENT MECHANIC WHO STATED THE FUEL INJECTOR SYSTEM WAS LEAKING AND THE O-RING NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 100,000.Read more
Incident date: Apr 13, 2010
TL* THE CONTACT OWNS A 1997 CHRYSLER CONCORD. THE CONTACT STATED WHILE DRIVING AT A SPEEDS OF 45 MPH, ENGINE COOLANT, WATER AND STEAM POURED FROM UNDER THE DASHBOARD AND INTO THE INTERIOR CABIN OF THE VEHICLE WITHOUT WARNING. BOTH THE DRIVER AND PASSENGER SUFFERED FIRST DEGREE BURNS TO BOTH FEET. TH
... IS WAS THE FIRST OCCURRENCE OF THE FAILURE. THE VEHICLE WAS TOWED TO THE DEALER FOR A DIAGNOSIS OF THE FAILURE. THE CONTACT HAD NOT YET RECEIVED THE RESULTS. THE CURRENT AND FAILURE MILEAGES WERE 48,000. UPDATED 05/19/10. *LJRead more
2 injured
Incident date: Oct 11, 2009
MY VEHICLE, DRIVEN BY MY STEP SON, CROSSED THE MEDIAN, SPUN AROUND AND SLAMMED BACKWARDS INTO A POWER POLE. HE HIT WITH ENOUGH FORCE TO PUSH THE REAR BUMPER AND THE TRUNK IN ALMOST 3 FEET AND YET THE AIR BAG DIDN'T DEPLOY. THE SUDDEN STOP BROKE THE FRONT SEAT LOOSE FROM THE FLOOR AND RIPPED HIS GL
... ASSES OFF HIS HEAD AND FLUNG THEM INTO THE BACK WINDOW. FORTUNATELY HE HAD HIS SEAT BELT ON, OR THE RECOIL WOULD HAVE SENT HIM THE FORWARD MOMENTUM FROM THE RECOIL WOULD HAVE SENT HIM THROUGH THE FRONT WINDOW. STILL THE AIR BAG DID NOT DEPLOY. THE ACCIDENT IS STILL UNDER INVESTIGATION AND IT IS UNCLEAR WHETHER HE WAS UNCONSCIOUS FOR A BRIEF PERIOD OF TIME FROM THE ACCIDENT.Read more
Crash
1 injured
Incident date: Jul 13, 2009
TL*THE CONTACT OWNS A 1997 CHRYSLER CONCORDE. THE CONTACT STATED THAT HE CAN REMOVE THE KEY FROM THE IGNITION WITHOUT PLACING THE VEHICLE INTO PARK. THE DEALER STATED THAT THE ISSUE WAS REPAIRED IN 2004, BUT HAS RECENTLY RECURRED. THE CONTACT WILL CHECK WITH THE MANUFACTURER FOR ASSISTANCE. THE
... FAILURE MILEAGE WAS 96,000.Read more
Incident date: Sep 30, 2008
BAD CRADLE BUSHINGS GRINDING NOISE WHEN DRIVING,TURNING,AND BREAKING LOUD BANG WHEN OVERDRIVE IS INITIATED AND VERY BAD ALIGNMENT FRONT DRIVER TIRE STARTED SMOKING AND THE BRAKE ROTOR WAS HOT ENOUGH TO BURN FLAT SPOTS ON MY FINGER TIPS. *TR
Incident date: Sep 30, 2008
BAD CRADLE BUSHINGS GRINDING NOISE WHEN DRIVING,TURNING,AND BREAKING LOUD BANG WHEN OVERDRIVE IS INITIATED AND VERY BAD ALIGNMENT FRONT DRIVER TIRE STARTED SMOKING AND THE BRAKE ROTOR WAS HOT ENOUGH TO BURN FLAT SPOTS ON MY FINGER TIPS. *TR
Incident date: Feb 14, 2009
I HAVE EXPERIENCED ALOT OF PLAY IN THE STEERING OF MY CHRYSLER CONCORDE 1997. AFTER INSPECTION IT WAS FOUND THAT THE FRONT CRADLE BUSHINGS WHERE WORN AWAY. I HAVE OWNED THIS CAR FOR 2 YEARS. I LOOKED AT A WEB SITE CONCERNING THIS AND OTHER PROBLEMS WITH THIS AND OTHER CHRSLER MODELS. AND IS CONCERNE
... D ABOUT THE ISSUES RELATED TO SEVERE AND CATASTROPHIC FAILURES WITH THESE VEHICLES. *TRRead more
Incident date: Feb 14, 2009
I HAVE EXPERIENCED ALOT OF PLAY IN THE STEERING OF MY CHRYSLER CONCORDE 1997. AFTER INSPECTION IT WAS FOUND THAT THE FRONT CRADLE BUSHINGS WHERE WORN AWAY. I HAVE OWNED THIS CAR FOR 2 YEARS. I LOOKED AT A WEB SITE CONCERNING THIS AND OTHER PROBLEMS WITH THIS AND OTHER CHRSLER MODELS. AND IS CONCERNE
... D ABOUT THE ISSUES RELATED TO SEVERE AND CATASTROPHIC FAILURES WITH THESE VEHICLES. *TRRead more
Incident date: Dec 5, 2008
I HAVE A 1997 CHRYSLER CONCORD. I HAD A SEVERE CLUNKING NOISE IN FRONT END. AFTER SEVERAL TRIPS TO THE GARAGE AND ALMOST $1000 LATER I HAD REPLACED BOTH INNER TIE ROD ENDS, ALL 4 CRADLE BUSHINGS AS WELL AS BOTH SWAYBARS IN FRONT END. NOT TO MENTION FRONT END ALIGNMENTS AFTER EACH REPAIR. THEN MY L
... EFT TIE ROD HAD TO BE REPLACED AGAIN WITHIN A BOUT A MONTH. THE PROBLEM WAS EVENTUALLY FIXED AND NOISE STOPPED UNTIL NOW. SIX MONTHS LATER I'M EXPERIENCING THE SAME NOISES AND A LOSE TIE ROD AGAIN. I HAVE SEEN ALL THE COMPLAINTS ABOUT CHRYSLER AND NOTE THAT THEY DON'T INCLUDE THE 1997 MODEL AS HAVING THESE PROBLEMS BUT I DO WITH MY 97 CONCORD. I HAVE 2 CHILDREN THAT RIDE IN MY VEHICLE AND THIS IS REALLY UNSAFE. IF THE TIERODS BREAK OR COME LOSE YOU CAN'T STEER THE CAR. THIS PROBLEM REALLY NEEDS TO BE ADDRESSED BY CHRYSLER AND FIXED. *TRRead more
Incident date: Aug 10, 2006
COMPLETE STEERING FAILURE ON 199 CHRYSLER CONCORDE. *TR
Incident date: Nov 1, 2007
OWN 1997 CHRYSLER CONDORDE. AC/EVAPORATOR ODOR. TECHNICAL SERVICE BULLETIN STATES GOING ON SINCE 1992 WITH CHRYSLER CARS. CAUSING AIRBORNE POLLUTANTS MIXED WITH BACTERIA AND FUNGI GROWTH. I HAVE ASTHMA, THIS IS A HEALTH ISSUE. CHRYSLER REGRETS THAT THEY HAVE NOTHING TO DO WITH THIS SINCE WART. UP .
... ISSUE IS THIS IS GOING ON SINCE 1992 WHY WAS THIS NOT ADDRESSED FOR SAFETY OF RESPIRATORY CONSUMERS. HEALTH HAZARD TO ALL WHO HAVE IMMUNE PROBLEMS. THIS WOULD NOT HAPPEN IN WART TIME PERIOD. THIS TAKES TIME TO FORM..END RESULTS MICROBIAL GROWTH ON EVAPORATOR CORE DURING NORMAL OPERATION, CONDENSATION FORMS IN AND AROUND AC EVAPORATOR. WHEN AIRBORNE POLLUTANTS MIX WITH CONDENSATION, BACTERIA AND FUNGI GROWTH BEGINS AND ODOR RESULTS. THIS IS THE RESPONSIBILITY OF CHRYSLER TO FIX AND MAKE CONSUMER SAFE AND NOT ENDANGERING THEIR HEALTH. WHY WAS THIS ISSUE NOT ADDRESSED IN 1992 ON WITH ALL THE REPORTS SHOWING THIS PROBLEM. CHRYSLER..CIRRUS,CONCORDE, NEW YORKER, IMPERIAL, LABARON COUPE,TOWN AND COUNTRY SEBRING VOYAGER ...SOMETHING IS WRONG WITH THIS PICTURE. WHO FAILED TO PICK UP ON THIS AND WHY SHOULD I HAVE TO PAY TO FIX SOMETHING THAT HAS BEEN GOING ON SINCE 1992 .JUST PURCHASED A 300C SPENDING $4,0000.00. NOW I WON'T KNOW IF THIS CAR WILL HAVE THE SAME PROBLEM IN FUTURE AND ENDANGER MY LIFE AS I HAVE ASTHMA AND THIS IS A RESPIRATORY PROBLEM. DISAPPOINTED CONSUMER WORRYING ABOUT MY HEALTH WITH THIS CAR. PLEASE HELP RESOLVE THIS PROBLEM.*TRRead more
Incident date: Feb 27, 2008
TL*THE CONTACT OWNS A 1997 CHRYSLER CONCORDE. WHILE DRIVING APPROXIMATELY 45 MPH, THE BACK OF THE DRIVER'S SEAT COLLAPSED BACKWARDS. THE FAILURE ALMOST CAUSED HER TO LOSE CONTROL OF THE STEERING. SHE DID NOT GET PULLED BACK ALONG WITH THE SEAT BECAUSE SHE WAS WEARING HER SEAT BELT. SHE FOUND A R
... ECALL FOR THIS FAILURE, BUT IT WAS FOR THE 1998 MODELS. THE MANUFACTURER STATED THAT HER VIN WAS NOT INCLUDED IN THE RECALL. THE FAILURE AND CURRENT MILEAGES WERE 174,000.Read more
Incident date: Oct 1, 2007
MY CAR STARTED MAKING A CLUNKING NOISE, AND I CHECKED OUT THE PROBLEM AND FOUND THE ENGINE CRADLE BUSHING WERE JUNK. THE CAR ONLY HAD 62000 MILES ON IT. THIS COULD OF CAUSED A VERY BAD ACCIDENT IF THE CRADLE HAD BROKEN. THE CAR WAS LIFTED OFF THE GROUND AND THERE WAS ABOUT A 2 IINCH GAP BETWEEN THE
... FRAME AND CRADLE WHERE THE BUSHING ARE WORN OUT. I CURRENT DON'T DRIVE THIS CAR DO TO THIS ISSUE.*CNRead more
Incident date: Oct 19, 2006
DT*: THE CONTACT STATED WHILE DRIVING 48 MPH, THE VEHICLE WAS HIT BY ANOTHER VEHICLE ON THE REAR PASSENGER SIDE. THE SEATBELT DID NOT AUTOMATICALLY LOCK, THE LENGTH OF THE BELT WAS NOT CONTROLLED BY THE SHOULDER BELT RETRACTOR. THE AUTOMATIC LOCKING RETRACTOR DID NOT FUNCTION AS IT SHOULD BE AND T
... HE PASSENGER IN THE REAR RIGHT SEAT OF THE VEHICLE SUSTAINED SERIOUS INJURIES. THERE WERE NO WARNING SIGNALS PRIOR TO THE INCIDENT. THE VEHICLE WAS TAKEN TO AN AUTO REPAIR SHOP.Read more
Crash
1 injured
Incident date: Jan 1, 2005
SAME SAD STORY AS THE OTHERS ON YOUR WEBSITE. I HAD A 1997 CHRYSLER CONCORDE. ON NEW YEAR'S DAY 2005 I WAS DRIVING TO MY DAUGHTER'S WHEN, WITHOUT WARNING, THE ENGINE BEGAN TO MAKE A KNOCKING NOISE. SUDDENLY, IT DIED. I HAD TOWED INTO MY DEALER, CLIFFORD CHRYSLER OF BUFFALO GROVE. THEY SAID THE ENGIN
... E HAD SEIZED UP DUE TO SLUDGE. SINCE THE CAR WAS JUST OUT OF WARRANTY INSISTED THEY TALK TO CHRYSLER. CHRYSLER SAID THE PROBLEM WAS CAUSED BY INADEQUATE OIL CHANGES EVEN WHEN I SENT THEM A RECORD OF MY OIL CHANGES, THEY REFUSED TO HELP WITH THE COST OF REPLACING THE ENGINE. *NMRead more
Incident date: Jun 9, 2006
AUTO-THEFT MECHANISM KICKED IN WHEN NOT NEEDED, RADIATOR AND AIR/CONDITIONER WENT OUT BEFORE 70,000 MILES AND NOW THE HEAD GASKET NEEDS REPLACING...AT 67,000 MILES. *JB
Incident date: Jun 9, 2006
AUTO-THEFT MECHANISM KICKED IN WHEN NOT NEEDED, RADIATOR AND AIR/CONDITIONER WENT OUT BEFORE 70,000 MILES AND NOW THE HEAD GASKET NEEDS REPLACING...AT 67,000 MILES. *JB
Incident date: Jun 9, 2006
AUTO-THEFT MECHANISM KICKED IN WHEN NOT NEEDED, RADIATOR AND AIR/CONDITIONER WENT OUT BEFORE 70,000 MILES AND NOW THE HEAD GASKET NEEDS REPLACING...AT 67,000 MILES. *JB
Incident date: Dec 1, 2003
CONSUMER 1997 CONCORDE DRIVER SIDE TIRE TURNED RIGHT WHILE DRIVING DOWN A HILL AND STOPPED. *TS AFTER HAVING THE VEHICLE TOWED, THE CONSUMER WAS INFORMED THE INNER TIE ROD HAD FAILED AND THE OUTER TIE ROD WAS ABOUT TO FAIL. THE DEALER STATED IT LOOKED AS IF THE VEHICLE HAD BEEN WORK ON PREVIOUSLY,
... AND WHOM EVER DID THE WORK DID NOT PLACE THE TABS BACK IN PLACE AND BECAUSE OF THAT THE TIE RODS EVENTUALLY STRIPPED AND FELL OUT OF PLACE. THE CONSUMER STATED THE RACK AND PINION WAS REPLACED AND THE PREVIOUS DEALER DID STATED THEY DID HAVE TO REMOVE THE TIE RODS IN ORDER TO REPLACE THE RACK AND PINION, HOWEVER THEY REFUSED TO REIMBURSE THE CONSUMER BECAUSE IT HAD BEEN OVER 5 YEARS SINCE THE REPAIR. *JBRead more
Incident date: Dec 25, 2003
ON CHRISTMAS DAY DRIVING WITH MY SON TO MY MOTHERS HOME ABOUT ONE HOUR AWAY, I EXITED THE FREEWAY AND STOPPED AT THE SIGNAL. WHEN THE SIGNAL TURNED GREEN, I PUSHED THE GAS, THE CAR DID NOT RESPOND. I CHECKED TO VERIFY THAT THE CAR WAS IN DRIVE. PUT THE CAR IN PARK, AND ATTEMPTED TO RESTART THE ENGIN
... E. THE ENGINE DID NOT RESPOND. THE VEHICLE WAS PUSHED TO A PARK AND RIDE, THEN TOWED TO THE DEALERSHIP. THE DEALERSHIP REPORTS THAT THE ENGINE SEIZED, AND IS DESTROYED BEYOND REPAIR OF THE VALUE OF THE VEHICLE. THERE WAS ZERO WARNING. THE VEHICLE DID NOT LOSE ANY FLUID. THERE WERE NOT ANY WARNING LIGHTS REGISTERING INSIDE THE VEHICLE. THE MAKE IS A CHRYSLER CONCORDE. IT IS A 1997, WITH 97,000 MILES. UP UNTIL THAT MOMENT THE VEHICLE WAS IDEAL. THEN WITHIN TEN FEET IT IS DESTROYED BEYOND REPAIR, WITHOUT ANY TYPE OF WARNING. *JBRead more
Incident date: Nov 22, 2005
WHEN I WOULD PLACE THE AUTOMATIC TRANSMISSION IN REVERSE ON MY 1997 CHRYSLER CONCORDE THE GAS PEDAL WOULD STICK AND ACCELERATE AT A RAPID RATE. THE ONLY WAY THAT I COULD STOP THE ACCELERATION WAS BY PLACING BOTH ON THE BRAKE AND TURNING THE KEY OFF. DAVE DENNIS CHRYSLER DEALER IN DAYTON, OH., VERIFI
... ED THIS. THEY FOUND THAT THE CRADLE BUSHINGS WERE BAD WHICH CAUSED THE MOTOR TO MOVE AND HIT THE THROTTLE WHICH CAUSED THE MOTOR TO REV. UP IN GEAR. THEY REPLACED THE CRADLE BUSHINGS AND I HAVE HAD NO TROUBLE SINCE. I CONSIDER THIS TO BE A SAFETY ISSUE. THE MECHANIC AT THE CHRYSLER DEALER STATED THAT WORN CRADLE BUSHINGS WERE A COMMON PROBLEM WITH K FRAMES USED ON CHRYSLERS. I CAN'T BE THE ONLY PERSON WHO HAS EXPERIENCED THIS PROBLEM DUE TO CRADLE BUSHINGS WEAR. *NMRead more
Incident date: Mar 30, 2003
DT: THE CONSUMER INDICATED THAT THE TIMING CHAIN BROKE WITHOUT WARNING. THIS HAS HAPPENED THREE TIMES AND EACH TIME THE CONSUMER HAD TO HAVE THE VEHICLE TOWED TO THE DEALER TO BE REPAIRED. THE MANUFACTURER SAID THERE IS NO RECALL ON THIS. THE CONSUMER SAID THAT THE ENGINE ALWAYS GETS REAL HOT A
... ND STALLS. SHE FORCED TO PULL OFF THE ROAD IN A DANGEROUS PLACES. *NMRead more
Incident date: Jun 1, 2005
PASSENGER SIDE AIRBAG COVER HAS DELAMINATED FROM METAL PORTION. APPEARS TO BE UNSAFE PASSENGER CONDITION.
Incident date: Jan 28, 2005
THE CONSUMER NOTICED THAT CAR SEEMED TO BE PULLING TO THE LEFT/RIGHT. THE CONSUMER HEARD SOMETHING POP AND RATTLE AND THEN PARTS STARTED FALLING FROM THE VEHICLE ON TO THE HIGHWAY. THE CONSUMER PURCHASED MORE PARTS AND THEY FAILED. THE CONSUMER TOOK THE VEHICLE TO MECHANIC WHO DETERMINED THE TRANSMI
... SSION FLUID LINE WAS LEAKING . ANOTHER MECHANIC STATED THAT THE FRONT END WAS COMING PART AND WAS LOOSE. THE FRAME WAS LOOSE AND NOTHING WAS HOLDING IT TOGETHER. AFTER REPLACING ALL THE PARTS, THE CONSUMER RECEIVED A RECALL NOTICE. TOOK IT TO DEALER AND THEY TOLD HER THAT THEY FIXED THE PROBLEM. BUT, DIDN'T TELL HER WHAT THE PROBLEM WAS, BUT NOW PROBLEM IS WORSE. CAR WAS JUMPING LIKE IT DIDN'T SHIFT INTO GEAR. TRANSMISSION FEELS LIKE IT'S SLIPPING. CONTACT CALLED NHTSA LAST WEEK AND TALKED TO A LADY AND WAS TOLD TO REPLACE THE POWER STEERING FLUID LINE. BOUGHT PIECE OF LINE AND WAS TOLD TO BUY A VACUUM PIPE.Read more
Incident date: May 1, 2005
THE ENGINE FAILED WHILE DRIVING, THE TEMP INDICATOR WENT FROM COLD TO HOT.
Incident date: Jan 28, 2005
THE CONSUMER NOTICED THAT CAR SEEMED TO BE PULLING TO THE LEFT/RIGHT. THE CONSUMER HEARD SOMETHING POP AND RATTLE AND THEN PARTS STARTED FALLING FROM THE VEHICLE ON TO THE HIGHWAY. THE CONSUMER PURCHASED MORE PARTS AND THEY FAILED. THE CONSUMER TOOK THE VEHICLE TO MECHANIC WHO DETERMINED THE TRANSMI
... SSION FLUID LINE WAS LEAKING . ANOTHER MECHANIC STATED THAT THE FRONT END WAS COMING PART AND WAS LOOSE. THE FRAME WAS LOOSE AND NOTHING WAS HOLDING IT TOGETHER. AFTER REPLACING ALL THE PARTS, THE CONSUMER RECEIVED A RECALL NOTICE. TOOK IT TO DEALER AND THEY TOLD HER THAT THEY FIXED THE PROBLEM. BUT, DIDN'T TELL HER WHAT THE PROBLEM WAS, BUT NOW PROBLEM IS WORSE. CAR WAS JUMPING LIKE IT DIDN'T SHIFT INTO GEAR. TRANSMISSION FEELS LIKE IT'S SLIPPING. CONTACT CALLED NHTSA LAST WEEK AND TALKED TO A LADY AND WAS TOLD TO REPLACE THE POWER STEERING FLUID LINE. BOUGHT PIECE OF LINE AND WAS TOLD TO BUY A VACUUM PIPE.Read more
Incident date: Jan 28, 2005
THE CONSUMER NOTICED THAT CAR SEEMED TO BE PULLING TO THE LEFT/RIGHT. THE CONSUMER HEARD SOMETHING POP AND RATTLE AND THEN PARTS STARTED FALLING FROM THE VEHICLE ON TO THE HIGHWAY. THE CONSUMER PURCHASED MORE PARTS AND THEY FAILED. THE CONSUMER TOOK THE VEHICLE TO MECHANIC WHO DETERMINED THE TRANSMI
... SSION FLUID LINE WAS LEAKING . ANOTHER MECHANIC STATED THAT THE FRONT END WAS COMING PART AND WAS LOOSE. THE FRAME WAS LOOSE AND NOTHING WAS HOLDING IT TOGETHER. AFTER REPLACING ALL THE PARTS, THE CONSUMER RECEIVED A RECALL NOTICE. TOOK IT TO DEALER AND THEY TOLD HER THAT THEY FIXED THE PROBLEM. BUT, DIDN'T TELL HER WHAT THE PROBLEM WAS, BUT NOW PROBLEM IS WORSE. CAR WAS JUMPING LIKE IT DIDN'T SHIFT INTO GEAR. TRANSMISSION FEELS LIKE IT'S SLIPPING. CONTACT CALLED NHTSA LAST WEEK AND TALKED TO A LADY AND WAS TOLD TO REPLACE THE POWER STEERING FLUID LINE. BOUGHT PIECE OF LINE AND WAS TOLD TO BUY A VACUUM PIPE.Read more
Incident date: Mar 1, 2005
1997 CHRYSLER CONCORDE EXPERIENCING PROBLEMS WITH DASH BOARD GAUGES AND LIGHTS BLINKING AND BECOMING INOPERATIVE.*MR *JB
Incident date: Oct 15, 2004
I WENT TO CREDIT CARS TO PURCHASE A VEHICLE KIND-OF LAST MINUTE. THEIR SALESMAN "ALFREDO" TOLD ME I NEEDED SOME ONE TO SIGN FOR "JOB LIABILITY." I TOLD HIM I DID NOT HAVE NOR WANT A CO-SIGNER. HE ASSURRED MY FRIEND/JOB LIABILITY SIGNER, CANDACE GULICK, THAT SHE WOULD NOT BE A CO-SIGNER. WE LATER FOU
... ND OUT THAT HE LIED. WHEN I DROVE MY CAR OFF THE LOT, CREDIT CARS AND I HAD AN AGREEMENT TO FIX THE NON-OPERATING GAGES. THEY ATTEMPTED TO FIX THEM 4 TIMES.(1 AT CREDIT CARS, 3 AT CAL-RICH AUTOMOTIVE) AFTER 4 ATTEMPTS AND NO LUCK, THOMAS FROM CREDIT CARS TOLD ME TO FIX THE 2 PROBLEMS WITH MY OWN MONEY, AND BECAUSE IT WAS ELECTRICAL HE DIDN'T HAVE TO FIX IT. WE HAD AN AGREEMENT BEFORE I BOUGHT THE CAR. (THE 2ND PROBLEM WAS I OPENED MY SUNROOF ONCE AND IT NEVER CLOSED AGAIN.) BECAUSE OF THE SUNROOF NOT CLOSING MY UPHOLSTERY MOLDED AND WAS RUINED. I DECIDED TO TAKE A TRIP A COUPLE OF HUNDRED MILES AWAY AND THE TRANSMISSION WENT OUT 10/15/2004 AND LEFT ME STRANDED. THIS WAS ONLY AFTER HAVING THE CAR FOR ALMOST 2MOS. I HAD A PRE-PAID LAWYER SERVICE WRITE THEM A LETTER AND ALL I RECEIVED WERE HARRASSING PHONE CALLS AT MY LAST JOB. I SPENT ALMOST $700.00 OF MY OWN MONEY TO TRY AND GET HOME WHEN THE "NEW" CAR LEFT ME STRANDED. MIND YOU THAT I AM A 21YR OLD FEMALE AND I WAS ALONE.*AKRead more
Incident date: Dec 1, 2004
THERE WERE SERIOUS SAFETY DEFECTS. THE A/C TURNS ON EVEN IF LOCKED OUT, THE DRIVER'S DOOR LEAKED, THE DASH LIGHTS BLINK ON/OFF WITHOUT CONTROL (ALL GAUGES), AND THE AIRBAG LIGHT, LIGHTS UP. BF THE TRUNK WOULD OPEN DUE TO MOISTURE IN THE AIR, AT NIGHT, THE WINDOW WOULD STEAM UP COMPLETELY IN SE
... CONDS, AND THE SPEEDOMETER WOULD QUIT. *SC *JBRead more
Incident date: Dec 1, 2004
THERE WERE SERIOUS SAFETY DEFECTS. THE A/C TURNS ON EVEN IF LOCKED OUT, THE DRIVER'S DOOR LEAKED, THE DASH LIGHTS BLINK ON/OFF WITHOUT CONTROL (ALL GAUGES), AND THE AIRBAG LIGHT, LIGHTS UP. BF THE TRUNK WOULD OPEN DUE TO MOISTURE IN THE AIR, AT NIGHT, THE WINDOW WOULD STEAM UP COMPLETELY IN SE
... CONDS, AND THE SPEEDOMETER WOULD QUIT. *SC *JBRead more
Incident date: Dec 1, 2004
THERE WERE SERIOUS SAFETY DEFECTS. THE A/C TURNS ON EVEN IF LOCKED OUT, THE DRIVER'S DOOR LEAKED, THE DASH LIGHTS BLINK ON/OFF WITHOUT CONTROL (ALL GAUGES), AND THE AIRBAG LIGHT, LIGHTS UP. BF THE TRUNK WOULD OPEN DUE TO MOISTURE IN THE AIR, AT NIGHT, THE WINDOW WOULD STEAM UP COMPLETELY IN SE
... CONDS, AND THE SPEEDOMETER WOULD QUIT. *SC *JBRead more
Incident date: Dec 1, 2004
THERE WERE SERIOUS SAFETY DEFECTS. THE A/C TURNS ON EVEN IF LOCKED OUT, THE DRIVER'S DOOR LEAKED, THE DASH LIGHTS BLINK ON/OFF WITHOUT CONTROL (ALL GAUGES), AND THE AIRBAG LIGHT, LIGHTS UP. BF THE TRUNK WOULD OPEN DUE TO MOISTURE IN THE AIR, AT NIGHT, THE WINDOW WOULD STEAM UP COMPLETELY IN SE
... CONDS, AND THE SPEEDOMETER WOULD QUIT. *SC *JBRead more
Incident date: Dec 1, 2004
THE CONSUMER STATED THAT WHILE DRIVING HE SMELLED A FUEL SMELL. THE CONSUMER WAS INFORMED THAT THE VEHICLE HAD A PROBLEM WITH THE O RINGS. CAMPAIGN ID NUMBER : 98V184000 *TC THIS PROBLEM MADE THE CONSUMER AND HIS WIFE EXTREMELY SICK. THE LEFT FRONT FUEL RAIL WAS FOUND LEAKING. *SC *JB
Incident date: Dec 29, 2004
(1) ALWAYS SMELLED GASOLINE AFTER DRIVING CAR FOR A WHILE. A COUPLE OF REPAIR PLACES COULD NOT FIND A PROBLEM. I FINALLY FIGURED OUT MYSELF WHERE THE LEAK WAS IN THE ENGINE AND POINTED IT OUT TO A REPAIR MAN. (2) THIS REPAIR MAN TOLD ME IT DEFINITELY WAS LEAKING AND IF I LET IT GO ANY LONGER THER
... E WOULD CERTAINLY BE AN ENGINE FIRE. WHEN I QUESTIONED HIM ABOUT OTHER OCCURRENCES OF THIS PROBLEM, HE SAID THAT HE HAD SEEN THIS HAPPEN MORE OFTEN ON CHRYSLER'S THAN ANY OTHER CAR. (3) HE REPLACED THE FUEL PRESSURE REGULATOR, AS WELL AS THE FUEL DAMPNER ASSEMBLY WITH FUEL RAIL. I DON'T HAVE THE OLD PARTS. LET ME KNOW IF YOU NEED THEM AND I WILL TRY TO OBTAIN THEM. *NMRead more
Incident date: Dec 1, 2004
WHILE TRAVELING CONSUMER SMELLED FUMES, AND IMMEDIATELY TOOK VEHICLE TO A DEALER SINCE HE FOUND OUT THERE WAS A RECALL FOR A FUEL RAIL. DEALER TOLD CONSUMER THAT THE RECALL WAS NOT ON DRIVER'S SIDE OF THE VEHICLE BUT ON PASSENGER'S SIDE.. NO RECALLS FOUND. *AK THE CUSTOMER WAS TOLD THAT TH
... E VEHICLE HAD A PROBLEM WITH THE O RINGS. RECALL FOUND: NHTSA CAMPAIGN ID NUMBER : 98V184000 RECALL DATE : AUG 06, 1998 *TCRead more
Incident date: Oct 19, 2004
THE CONSUMER RECEIVED A RECALL(NHTSA 98V184000) REGARDING THE FUEL RAIL. THE DEALER REFUSED TO PERFORM THE RECALL. *JB
Incident date: Oct 12, 2004
WHILE BACKING OUT OF THE GARAGE, WITHOUT WARNING THE VEHICLE CAUGHT FIRE. THE CONSUMER EXTINGUISHED THE FIRE OUT AND THE VEHICLE WAS PUSHED BACK INTO THE GARAGE. THE DRIVER HAS CONTACTED THE DEALER FOR INSPECTION AND A APPOINTMENT. THE RECALL WAS NOT FOR THIS VEHICLE. PLEASE FILL IN ADDITIONAL I
... NFORMATION. *JBRead more
Fire
Incident date: Jul 24, 2004
FIRST, IT STARTED OUT WITH THE CRACKED FUEL RAIL PROBLEM WHICH COST US OVER 900.00 TO REMEDY AND EVER SINCE WE HAVE HAD NOTHING BUT PROBLEMS WITH IT NOT WANTING TO IDLE SO WE REPLACED THE IDLE CONTOL AT THE COST OF OVER 60.00 WHICH STILL HASN'T FIXED THE ISSUE. THE SCANS BEING DONE SHOW A MISFIRE IN
... CYLINDER #5 BUT ALSO CAN'T BE REMEDIED. YOU CAN BE DRIVING ALONG AT HIGHWAY SPEEDS AND ALL OF A SUDDEN IT BUCKS WILDLY, THE TACHOMETER SWINGS WILDLY THEN IT JUST STALLS AND WON'T RESTART. THE EGR VALVE AT A COST OF OVER 114.00. PROBLEM STILL EXISTS. NOONE CAN SEEM TO FIND A RESOLVE TO THIS ISSUE. THIS HAS TURNED MY VEHICLE INTO A VERY UNRELIABLE MEANS OF TRANSPORTATION AND I WON'T PERMIT MY WIFE TO DRIVE IT ANY LONGER, YET WE ARE FORCED TO CONTINUE MAKING OUR PAYMENTS OR HAVE IT REPOSSESED. THIS HAS BEEN GOING ON NOW FOR AT LEAST FOUR MONTHS WITH US NURSING THE VEHICLE JUST TO DRIVE THE TEN MILES TO WORK WITH SEVERAL STOPPAGES ALONG THE WAY.*AKRead more
Incident date: Jun 3, 2004
WHILE DRIVING THE VEHICLE A LITTLE WHILE, HALF OF THE ENGINE OVERHEATED AND THE OTHER HALF WAS A NORMAL TEMPERATURE. THE VEHICLE WAS TAKEN TO A DEALERSHIP. THEY REPLACED THE LIFTER AND VALVE ON THE DRIVER'S HEAD AT THE OWNER'S EXPENSE. *NM
Incident date: Feb 9, 2004
WHILE DRIVING AT 40 MPH THE VEHICLE COLLIDED WITH ANOTHER VEHICLE HEAD ON. THE CONSUMER SUFFERED A HERNIATED DISC IN THE BACK AND LEG AND LEG MUSCLE SPRAINS. THE POLICE ARRIVED AND CITED THE CONSUMER FOR DRIVING IN A SAFETY ZONE. THE CONSUMER WAS WEARING A SEAT BELT AT THE TIME BUT THE AIRS BAG D
... ID NOT DEPLOY. *NMRead more
Crash
1 injured
Incident date: Jun 11, 2002
IN 2002 OUR CAR OVERHEATED WE TOOK IT INTO A REPAIR SHOP. SINCE THE IT IT WAS BOUGHT IN ON FOUR DIFFERENT OCCASIONS TO REPAIR THE COOLING SYSTEM, OVER A SPAN OF LESS THAN A YEAR. THE ENTIRE COLLING SYSTEM, EXCEPT FOR THE HEATING COIL HAS BEEN REPLACED. THEN THE CHECK ENGINE LIGHT CAME ON. IT HA
... S HAD A MISFIRE IN CYLINDER #5 AND WE HAVE SUNK IN OVER A $1,000 AND THE PROBLEM IS STILL NOT FIXED. THE MECHANICS HAVE TOLD US THEY CAN'T FIND WHAT IS CAUSING IT. THE LIGHT HAS BEEN ON FOR OVER EIGHT MONTHS. IT HAS BEEN HOOKED UP TO COMPUTERS AND STILL IT IS A GUESSING GAME. WE HAVE HAD THE EGR VALVE REPLACED BECAUSE THIS WAS ANOTHER GUESS AS TO THE PROBLEM. WE HAVE ALSO REPLACED THE FUEL INJECTORS, SPARK PLUGS, WIRES, COIL, OVERHEAD CAM SENSOR, IDLE AIR CONTROL VALVE AND TIMING BELT. WE ARE SINKING MORE MONEY INTO THIS CAR THAN WE CAN AFFORD. IF THERE IS A PROBLEM WITH THIS CAR WE SHOULD HAVE BEEN MADE AWARE OF IT BEFORE WE PURCHASED IT. WE HAVE TAKEN IT TO THREE DIFFERENT MECHANICS AND STILL NO-ONE CAN TELL US WHAT THE PROBLEM IS. ANY HELP YOU CAN GIVE US WOULD BE GREATLY APPRECIATED.*AKRead more
Incident date: Jun 11, 2002
IN 2002 OUR CAR OVERHEATED WE TOOK IT INTO A REPAIR SHOP. SINCE THE IT IT WAS BOUGHT IN ON FOUR DIFFERENT OCCASIONS TO REPAIR THE COOLING SYSTEM, OVER A SPAN OF LESS THAN A YEAR. THE ENTIRE COLLING SYSTEM, EXCEPT FOR THE HEATING COIL HAS BEEN REPLACED. THEN THE CHECK ENGINE LIGHT CAME ON. IT HA
... S HAD A MISFIRE IN CYLINDER #5 AND WE HAVE SUNK IN OVER A $1,000 AND THE PROBLEM IS STILL NOT FIXED. THE MECHANICS HAVE TOLD US THEY CAN'T FIND WHAT IS CAUSING IT. THE LIGHT HAS BEEN ON FOR OVER EIGHT MONTHS. IT HAS BEEN HOOKED UP TO COMPUTERS AND STILL IT IS A GUESSING GAME. WE HAVE HAD THE EGR VALVE REPLACED BECAUSE THIS WAS ANOTHER GUESS AS TO THE PROBLEM. WE HAVE ALSO REPLACED THE FUEL INJECTORS, SPARK PLUGS, WIRES, COIL, OVERHEAD CAM SENSOR, IDLE AIR CONTROL VALVE AND TIMING BELT. WE ARE SINKING MORE MONEY INTO THIS CAR THAN WE CAN AFFORD. IF THERE IS A PROBLEM WITH THIS CAR WE SHOULD HAVE BEEN MADE AWARE OF IT BEFORE WE PURCHASED IT. WE HAVE TAKEN IT TO THREE DIFFERENT MECHANICS AND STILL NO-ONE CAN TELL US WHAT THE PROBLEM IS. ANY HELP YOU CAN GIVE US WOULD BE GREATLY APPRECIATED.*AKRead more
Incident date: Jan 21, 2004
WHILE DRIVING 70 MPH ENGINE FAILED.*AK
Incident date: Jun 15, 2003
WATER LEAKS UNDER AIR VENTS UNDER WINDOW WIPERS ,BODY SEAMS LET WATER IN CAR AS FAST AS IT WILL RUN.HAVE SEALED 1 LEAK WITH SILICONE ON SEAM ON PASSENGER SIDE. CARPET AND MAT ON DRIVER SIDE NOW GETTING WET AND STINKS. REPLACED WINDSHIELD 6-27-03,SO I KNOW THAT WAS NOT THE PROBLEM. CAR BOUGHT NEW AND
... HAS NEVER BEEN IN ACCIDENT. DEALERS SERVICE MGR.CLAIMS THERE HAS NOT BEEN ANY PROBLEMS,BUT MY MECHANIC,KNOWS A CHRYSLER MECHANIC THERE,AND HE SAYS THERE ARE PLENTY OF COMPLAINTS. THEY HAVE EVEN SPRAYED RUBBERIZED UNDERCOATING ON SEAMS AND SURROUNDING AREAS TO SEAL WATER LEAKS.Read more
Incident date: Apr 6, 2004
WHILE REVERSE OUT OF THE DRIVEWAY AT LOW SPEEDS VEHICLE ACCELERATED TO A HIGH SPEED. ALSO, WHEN BRAKING THERE WAS EXTENDED STOPPING DISTANCE. DEALERSHIP WILL BE NOTIFIED. *AK
Incident date: Apr 6, 2004
WHILE REVERSE OUT OF THE DRIVEWAY AT LOW SPEEDS VEHICLE ACCELERATED TO A HIGH SPEED. ALSO, WHEN BRAKING THERE WAS EXTENDED STOPPING DISTANCE. DEALERSHIP WILL BE NOTIFIED. *AK
Incident date: Feb 19, 2004
WHILE DRIVING 40 MPH ENGINE FAILED WITHOUT WARNING. *AK
Incident date: Jan 13, 2004
POWER STEERING IS OUT OR VERY HARD TO TURN UNTIL THE CAR IS WARMED UP. I BOUGHT THIS CAR IN AUG. OF 2003. THIS HAS FAILED ATLEAST 120 TIMES. DOESN'T MATTER IF IT IS SUMMER OR WINTER. WAS CHECKING TO SEE IF THIS WAS RECALLED. IT WASN'T SO I MADE A COMPLAINT.
Showing 50 of 189 complaints.