EXXONMOBIL PIPELINE CO
hazardous_liquid Incident — — April 14, 2010
Incident Information
| Incident Date | April 14, 2010 |
| Operator | EXXONMOBIL PIPELINE CO |
| Commodity | CRUDE OIL |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 32.47413, -94.71850 |
Cause
| Cause | CORROSION FAILURE |
| Subcause | INTERNAL CORROSION |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $0 |
| Emergency Response | $5,000 |
| Other Costs | $0 |
Location Map
Incident Narrative
"RELEASE OCCURRED ON IDLE PIPING AT LONGVIEW STATION, LONGVIEW, TEXAS. THE IDLE LINE WAS ONCE ATTACHED TO STATE LINE TO MIDVALLEY CRUDE SYSTEM. SUPPLEMENTAL REPORT.-1-31-11 IDLE PIPE HAS NOT BEEN REMOVED AND FINAL INVESTIGATION CAN NOT BE COMPLETED UNTIL THE PIPE IS REMOVED FROM THE GROUND TO DETERMINE OF THE LEAK WAS INTERNAL OR EXTERNAL. PRODUCT WAS REMOVED WHEN THE LEAK OCCURRED ON 4/14/2010. THE PIPE IS DRY AND AWAITING REMOVAL. PIPE REMOVAL IS ANTICIPATED BEFORE MARCH 31, 2011. 7001 REVISED DATE IS 1-31-11 SUPPLEMENTAL AND FINAL REPORT 4- 21-11 AFTER REMOVAL OF THE PIPE AT THE LEAK SITE ON MARCH 18, 2011, THE LEAK CAUSE WAS DETERMINED TO BE INTERNAL CORROSION. SECTION G OF THE 7001 FORM HAS BEEN UPDATED WITH INTERNAL CORROSION INFORMATION. INVESTIGATION IS COMPLETE AND 7001 REPORT IS FINAL. 4-21-11 SUPPLEMENTAL REPORT 7-30-13 PHMSA REQUESTED SUPPLEMENTAL BE CREATED TO ADDED PART E 5 F DATA IE, ( FUNCTION OF PIPELINE SYSTEM) BE ADDED TO FORM."
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.