COLONIAL PIPELINE CO

hazardous_liquid Incident — — December 6, 2010

Incident Information

Incident DateDecember 6, 2010
OperatorCOLONIAL PIPELINE CO
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates39.36139, -77.03778

Cause

CauseINCORRECT OPERATION
Subcause"VALVE LEFT OR PLACED IN WRONG POSITION, BUT NOT RESULTING IN A TANK, VESSEL, OR SUMP/SEPARATOR OVERFLOW OR FACILITY OVERPRESSURE"

Casualties

Fatalities0
Injuries0

Costs

Property Damage$2,500
Emergency Response$7,745
Other Costs$0

Location Map

Incident Narrative

"ON MONDAY, DECEMBER 6, 2010 AT 07:30, AN OPERATOR DISCOVERED THE DORSEY 03 BOOSTER STATION SUMP HAD PRODUCT ON THE LID AND A GRAVEL STAINED AREA. APPROPRIATE NOTIFICATIONS WERE MADE. TWO NEARBY ACCESS WELLS HAD PRODUCT IN THEM. THE INITIAL INVESTIGATION FOUND THE SUMP DISCHARGE VALVE IN THE CLOSED POSITION. NIGHT SHIFT OPERATORS HAD PUMPED THE SUMP AROUND 6 AM. THE LEVEL WAS APPROXIMATELY 1.2'. THE SITE WAS EXCAVATED AND CONTAMINATED SOIL SECURED FOR DISPOSAL. THE SUMP PUMP SEAL FAILED, CAUSING THE PRODUCT RELEASE. REPAIRS WERE COMPLETED THE SAME DAY AND THE EQUIPMENT WAS RETURNED TO SERVICE."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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