UNOCAL PIPELINE CO - EASTERN REGION

hazardous_liquid Incident — — December 6, 2010

Incident Information

Incident DateDecember 6, 2010
OperatorUNOCAL PIPELINE CO - EASTERN REGION
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates32.54060, -95.70117

Cause

CauseCORROSION FAILURE
SubcauseEXTERNAL CORROSION

Casualties

Fatalities0
Injuries0

Costs

Property Damage$15,000
Emergency Response$200,000
Other Costs$0

Location Map

Incident Narrative

"AT 1500 CST ON 06 DEC 10 CPL FIELD PERSONNEL CONFIRMED A RELEASE ON THE 8"" VAN GATHERING SYSTEM NEAR THE VAN STATION. THE RELEASE SOURCE WAS A PINHOLE @ THE 6 O' CLOCK POSITION; DIRECTLY BELOW THE LINE IS A SEWER OPENING THAT FEEDS TO A NEARBY WATER TREATMENT FACILITY. THERE ARE REPORTS OF AN OIL SHEEN IN THE TREATMENT FACILITY. CHEVRON PRODUCTION AND CPL PERSONNEL HAVE DEPLOYED SKIMMER UNITS AND A VACUUM TRUCK @ THE TREATMENT FACILITY; CONTAINMENT BOOM, SKIMMER UNITS AND A VACUUM TRUCK HAVE BEEN DEPLOYED @ THE LITTLE SANDY CREEK OUTFALL AREA, THE POINT OF DISCHARGE FROM THE TREATMENT FACILITY. CPL CREW INSTALLED A TEMPORARY CLAMP TO PREVENT FURTHER LEAKAGE. THE FOLLOWING DAY, CPL CREW REMOVED TEMPORARY CLAMP & INSTALLED A PLIDCO MECHANICAL SLEEVE. THE SEWAGE TREATMENT PLANT AND PIPING HAVE BEEN CLEANED OF ALL CONTAMINATES. THE SECTION OF PIPE WHERE THE LEAK OCCURRED WILL REMAIN OUT OF SERVICE UNTIL FURTHER NOTICE. CPL HAS MADE THE DECISION TO IDLE THE ENTIRE VAN CRUDE SYSTEM & WE ARE CURRENTLY IN THE PROCESS OF REMOVING THE CRUDE OIL LINE FILL."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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