"MAGELLAN PIPELINE COMPANY, LP"

hazardous_liquid Incident — — February 24, 2011

Incident Information

Incident DateFebruary 24, 2011
Operator"MAGELLAN PIPELINE COMPANY, LP"
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates29.40090, -94.95689

Cause

CauseMATERIAL FAILURE OF PIPE OR WELD
SubcauseORIGINAL MANUFACTURING-RELATED (NOT GIRTH WELD OR OTHER WELDS FORMED IN THE FIELD)

Casualties

Fatalities0
Injuries0

Costs

Property Damage$403,000
Emergency Response$149,000
Other Costs$0

Location Map

Incident Narrative

"THE PIPELINE WAS OPERATING AT STEADY STATE PRIOR TO THE EVENT AT APPROXIMATELY 10,000 BPH. NO ABNORMAL OPERATING CONDITIONS OCCURRED IMMEDIATELY PRIOR TO THE EVENT. THE PIPELINE CONTROLLER VIA SCADA RECEIVED AN ALERT OF HIGH FLOWRATE AND LOW DISCHARGE PRESSURE. THE PIPELINE WAS PROMPTLY SHUTDOWN AND REMOTELY OPERATED VALVES CLOSED. UPON INVESTIGATION IT WAS DISCOVERED THAT PIPELINE LONG SEAM HAD SPLIT ON TOP OF THE PIPE. FURTHER METALURGICAL ANALYSIS DETERMINED IT WAS A DAMAGED SKELP EDGE DURING MANUFACTURING THAT CAUSED A LACK OF BONDING. - SEE ANALYSIS ATTACHED. REMOVED PART A #10 AS INSTRUCTED BY EMAIL OF PIYALI TALUKDAR ON 2/28/13. SUPPLEMENTAL/FINAL (02/11/2020) UPDATED G5-1 TO REMOVE ""UNDER INVESTIGATION"""

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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