PORTLAND PIPELINE CORP
hazardous_liquid Incident — — January 4, 2010
Incident Information
| Incident Date | January 4, 2010 |
| Operator | PORTLAND PIPELINE CORP |
| Commodity | CRUDE OIL |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 43.94028, -70.49336 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | PUMP OR PUMP-RELATED EQUIPMENT |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $4,000 |
| Emergency Response | $0 |
| Other Costs | $0 |
Location Map
Incident Narrative
APPROXIMATELY 5 GALLONS OF CRUDE OIL OVERFLOWED FROM THE PUMP SEAL SCAVENGER BOX OF AN OUTDOOR MAIN LINE PUMP UNIT. THE OIL WAS CONFINED TO THE CRUSHED STONE AND SNOW-COVERED GROUND IMMEDIATELY ADJACENT TO THE PUMP UNIT ON THE PUMP STATION PROPERTY. NO OIL ESCAPED COMPANY PROPERTY OR REACHED SURFACE WATERS. THE OIL WAS DISCOVERED DURING THE NEXT SCHEDULED INSPECTION, AND THE PUMP UNIT WAS IMMEDIATELY SHUT DOWN. ALL OIL WAS RECOVERED BY HAND AND VACUUM EXCAVATION OF THE OILED SNOW, CRUSHED STONE, AND SOIL; THE RECOVERED MATERIALS WERE RECYCLED. THE CAUSE OF THE SCAVENGER BOX OVERFLOW WAS THAT THE DRAIN LINE FROM THE SCAVENGER BOX HAD BECOME PARTIALLY PLUGGED WITH SANDY SEDIMENT FROM THE CRUDE OIL BEING PUMPED, AND IN THE SUBSEQUENT COLD WEATHER THE CRUDE OIL DRAINING THROUGH THE LINE CONGEALED AROUND THE SEDIMENT, BLOCKING THE DRAIN. AFTER THE INCIDENT, THE DRAIN LINE WAS DISASSEMBLED, THOROUGHLY CLEANED, AND REINSTALLED. THE PUMP WAS ALSO DISASSEMBLED AND THE SEALS WERE INSPECTED AND REPLACED WITH NEW PARTS TO REDUCE THE LEAKAGE THROUGH THE SEAL, THOUGH THE LEVEL OF WEAR WAS NOT UNUSUAL.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.