ENTERPRISE PRODUCTS OPERATING LLC
hazardous_liquid Incident — — September 11, 2011
Incident Information
| Incident Date | September 11, 2011 |
| Operator | ENTERPRISE PRODUCTS OPERATING LLC |
| Commodity | HVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 38.38052, -97.83095 |
Cause
| Cause | INCORRECT OPERATION |
| Subcause | PIPELINE OR EQUIPMENT OVERPRESSURED |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $0 |
| Emergency Response | $0 |
| Other Costs | $0 |
Location Map
Incident Narrative
"WHILE ESTABLISHING FLOW FROM A CUSTOMER'S INBOUND LINE SEGMENT TO A DOWNSTREAM CUSTOMER'S FACILITY, PIPING INSIDE THE OPERATOR'S FACILITY WAS OVER-PRESSURED FOR A BRIEF PERIOD OF TIME BEFORE THE OPERATOR'S SHUT DOWN VALVE (SDV) CLOSED COMPLETELY. A SMALL THERMAL RELIEF VALVE ON THE OPERATOR'S FACILITY OPENED AT SET POINT DURING THIS TIME FRAME AND RELEASED AN ESTIMATED 7.3 GALLONS OF PROPANE TO THE ATMOSPHERE. PER THE OPERATOR'S INCIDENT INVESTIGATION, IT APPEARS THAT THE DOWNSTREAM CUSTOMER INFORMED THE OPERATOR THAT THE DOWNSTREAM CUSTOMER WAS READY TO RECEIVE PRODUCT WHEN, IN FACT, A VALVE IN THE FLOW PATH INSIDE THE DOWNSTREAM CUSTOMER'S FACILITY WAS NOT OPEN WHEN THE OPERATOR INITIATED FLOW FROM THE INBOUND LINE SEGMENT. THE OPERATOR'S SDV SETPOINT HAS BEEN LOWERED TO PREVENT THE THERMAL RELIEF VALVE FROM RELIEVING DURING A SURGE CONDITION."
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.