LOOP INC

hazardous_liquid Incident — — January 25, 2010

Incident Information

Incident DateJanuary 25, 2010
OperatorLOOP INC
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates29.47000, -90.25444

Cause

CauseEQUIPMENT FAILURE
SubcauseFAILURE OF EQUIPMENT BODY (EXCEPT PUMP), TANK PLATE, OR OTHER MATERIAL

Casualties

Fatalities0
Injuries0

Costs

Property Damage$30,000
Emergency Response$600,000
Other Costs$0

Location Map

Incident Narrative

THE SUMP AT THE LOOP LLC CLOVELLY DOME STORAGE TERMINAL INJECTION STATION OVERFLOWED WHEN A VALVE ON A 6-INCH DRAIN LINE ALLOWED FLOW BACK INTO THE SUMP AT A RATE TOO HIGH FOR THE PUMPS TO MAINTAIN. THE PRELIMINARY INVESTIGATION INDICATES THAT THE VALVE MAY NOT HAVE SEATED PROPERLY WHEN LAST OPERATED AND THAT THIS MALFUNCTION WAS NOT DETECHED AT THE TIME DUE TO SEDIMENT BUILDUP IN THE DRAIN LINE AS IT IS RARELY USED. IT IS THOUGHT THAT THE SEDIMENT BLOCKAGE BROKE LOOSE ALLOWING OIL TO FLOW INTO THE SUMP THROUGH THE PARTIALLY OPENED VALVE. AN INVESTIGATION TEAM HAS BEEN COMMISSIONED TO CONDUCT A MORE THOROUGH CASUAL ANALYSIS OF THE ACCIDENT. THE INVESTIGATION TEAM COMPLETED THE CAUSAL ANALYSIS REFERENCED ABOVE AND CONCURRED THAT THE PRIMARY CAUSE OF THE SPILL WAS THE SEDIMENT BUILDUP BREAKING LOOSE ALLOWING OIL TO FLOW THROUGH THE IMPROPERLY SEATED VALVE INTO THE SUMP.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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