DENBURY GREEN PIPELINE-TEXAS, LLC

hazardous_liquid Incident — — February 14, 2011

Incident Information

Incident DateFebruary 14, 2011
OperatorDENBURY GREEN PIPELINE-TEXAS, LLC
CommodityCO2 (CARBON DIOXIDE)
Pipeline Typehazardous_liquid

Location

State
Coordinates29.98722, -94.07171

Cause

CauseMATERIAL FAILURE OF PIPE OR WELD
SubcauseORIGINAL MANUFACTURING-RELATED (NOT GIRTH WELD OR OTHER WELDS FORMED IN THE FIELD)

Casualties

Fatalities0
Injuries0

Costs

Property Damage$64,111
Emergency Response$2,520
Other Costs$0

Location Map

Incident Narrative

ON FEBRUARY 14, 2011 A CONTRACT SURVEY CREW NOTICED INDICATIONS OF A POTENTIAL LEAK ON A DENBURY RIGHT-OF-WAY NEAR BEAUMONT, TEXAS. THEY REPORTED THE LEAK TO DENBURY OPERATIONS AND REGULATORY PERSONNEL AT APPROXIMATELY 1:00PM. UPON FURTHER INVESTIGATION, THE LOCATION OF THE POTENTIAL LEAK WAS AT A CROSSING WITH TWO OTHER PIPELINES. DENBURY ELECTED TO HAVE A CONTRACTOR EXCAVATE TO CONFIRM THAT THE LEAK WAS FROM OUR PIPELINE OR FROM ANOTHER SOURCE. IT WAS CONFIRMED THAT THE LEAK WAS FROM DENBURY'S PIPELINE AT 5:30PM. THE INITIAL COST TO REPAIR THE LEAK WAS ESTIMATED AT $90,000, WHICH WOULD REQUIRE NATIONAL RESPONSE CENTER TELEPHONIC REPORTING. THE NRC REPORT WAS ELECTRONICALLY SUBMITTED AT 7:12PM. THE LEAK RATE WAS ESTIMATED AT 2 GALLONS PER HOUR. ISOLATION OF THE LINE SEGMENT WAS ACCOMPLISHED ON FEBRUARY 16, 2011 AT 4:00PM. THE LINE WAS BLOWN DOWN FROM MLV-22 TO THE BEAUMONT STATION (15.8 MILES). ON FEBRUARY 17, 2011, TROY CONSTRUCTION BEGAN LINE REPAIR WORK. OTHER PROJECT DETAILS AND LOGISTICS WERE CONFIRMED, INCLUDING MOVING PRE-TESTED PIPE FROM THE WINNIE, TEXAS YARD TO THE JOBSITE AND MAKING COATING REPAIRS TO THE PRE-TESTED PIPE. OQ AND DRUG AND ALCOHOL PLANS WERE CONFIRMED WITH ALL PARTICIPATING CONTRACTORS AND THEIR PERSONNEL. WITH BLOWDOWN OF THE LINE COMPLETE AND A PRE-JOB SAFETY MEETING CONDUCTED, AIR MOVERS WERE INSTALLED AT MLV-24 AND BEAUMONT STATION IN PREPARATION TO REPLACE LEAKING PIPE 300 YARDS EAST OF BEAUMONT STATION. REMOVED THE LEAKING 24' 46' LONG JOINT AND MADE 1 WELD ON REPLACING PIPE. X-RAY WAS ACCEPTED. MADE SECOND TIE IN WELD ON NEW SECTION OF PIPE. X-RAY WAS ACCEPTED. DOPED AND WRAPPED WELDS AND BACKFILLED. STARTED RE-COMMISSIONING GREEN PIPELINE FROM MLV-22 TO BEAUMONT STATION ON FEBRUARY 18, 2011 AT 1:20PM. PIPELINE WAS BACK IN SERVICE ON FEBRUARY 19, 2011 AT 5:18AM.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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