"SFPP, LP"
hazardous_liquid Incident — — January 8, 2013
Incident Information
| Incident Date | January 8, 2013 |
| Operator | "SFPP, LP" |
| Commodity | REFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 38.56947, -121.52266 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | OTHER EQUIPMENT FAILURE |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $100 |
| Emergency Response | $2,000 |
| Other Costs | $0 |
Location Map
Incident Narrative
"ON 1/8 A TANK CONTRACTOR NOTIFIED KM PERSONNEL OF A POSSIBLE RELEASE AT OUR SACRAMENTO STATION. AT 0957, KINDER MORGAN TECHNICIANS CONFIRMED THE RELEASE FROM FAILED VALVE PACKING ON MOV-1. THE ESTIMATED VOLUME OF THE RELEASE USING L-O&M 159 WAS ESTIMATED TO BE 9.3 GALLONS. THE LINE WAS SHUTDOWN, CA (AGENCY) LEAK NOTIFICATIONS WERE MADE AND AN INTERNAL ERL CALL WAS CONDUCTED. THE VALVE WAS REPACKED, IMPACTED SOIL WAS EXCAVATED AND PLACED INTO THREE LABELED DRUMS BY THE MAINTENANCE CREW AND THE EXCAVATION WAS BACKFILLED."
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.