ENBRIDGE ENERGY, LIMITED PARTNERSHIP

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENBRIDGE ENERGY, LIMITED PARTNERSHIP
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates41.50506, -87.45430

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

TANK 1607 WAS TAKEN OUT OF SERVICE IN ORDER TO PERFORM AN API 653 INSPECTION. THE TANK VALVE WAS REMOVED AND A BLIND FLANGE WAS INSTALLED (ON THE TANK SIDE END OF THE PIPING ASSEMBLY). TANK LINE HAD A CLAMP (DRESSER COUPLING) WITHIN THE TANK LINE PIPE ASSEMBLY. ON OCTOBOER 12, 2011 THE DRESSER COUPLING CONNECTION FAILED AND APPROXIMATELY 398 BARRELS OF OIL WAS RELEASED FROM THE PIPE COUPLING CONNECTION INTO THE BERM AREA. TANK INSPECTION WORK AT THE HARTSDALE TERMINAL WAS HALTED AND CREWS COMMENCED CLEAN UP AND TEMPORARY REPAIRS ON THE FAILED SECTION. AN INCIDENT INVESTIGATION COMMENCED AND IS ONGOING TO DETERMINE THE ROOT CAUSE AND POTENTIAL CONTRIBUTING FACTORS. CLEAN UP OF THE SITE HAS BEEN COMPLETED. UPDATE AUG 2012 THERE ARE TWO PRIMARY CAUSES FOR THIS INCIDENT: -LACK OF ADEQUATE LONGITUDINAL ANCHORAGE: THE LACK OF SUFFICIENT ANCHORAGE ALLOWED THE BLIND FLANGE PIPE PIECE TO SLIP OUT OF THE DRESSER COUPLING WHICH RESULTED IN A RELEASE OF CRUDE OIL WHEN THE LINE WAS PRESSURIZED. THE ANCHORAGE PROVIDED TO THE DRESSER COUPLING WAS TWO CHAINS, WHICH SPANNED ACROSS THE COUPLING AND WERE WELDED TO PIPES ON EACH SIDE. THESE CHAINS WERE NOT CAPABLE OF RESISTING THE END CAP FORCE GENERATED BY PRESSURE UP TO THE RATED CAPACITY OF THE FILL LINE PIPING (182 PSI). -FAILURE TO ISOLATE THE OUT-OF-SERVICE TANK LINE :THE DESIRED DOUBLE BLOCK AND BLEED CONDITION WAS COMPROMISED BY LEAVING THE ISOLATION VALVE THAT WAS CONNECTED TO THE TERMINAL MANIFOLD PARTIALLY OPEN FOR THERMAL RELIEF, WHILE EXECUTING A MANEUVER THAT PRESSURIZED THE MANIFOLD. UPDATE MAY 2013 APPROXIMATELY 512 TONS OF CONTAMINATED SOIL WAS REMOVED FROM THE SITE AND DISPOSED OF AT AN APPROVED LOCATION.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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