SHELL PIPELINE CO., L.P.
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | SHELL PIPELINE CO., L.P. |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 30.01111, -90.83889 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
SMALL STAINLESS STEEL TUBING FAILURE AT CONNECTION TO PRESSURE TRANSMITTER FITTING. TUBING WAS ISOLATED BY CLOSING VALVE. CONTINUE TO OPERATE PIPELINE. CORRECTIVE ACTION TAKEN - MOVED PRESSURE TRANSMITTER TO ELIMINATE THE SS TUBING. ALL CRUDE OIL RELEASED WAS TO SECONDARY CONTAINMENT, CONCRETE AREA. ALL CRUDE OIL WAS RECOVERED. NO CONTACT WITH SOIL. PART A - NRC REPORT NUMBER 1000974. NOT ABLE TO INPUT 7 DIGITS IN FORM. 3/13/2013 - UPDATED E5F PER REQUEST FROM PHMSA. 6/6/2013 - UPDATED HCA DW
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.