ENTERPRISE PRODUCTS OPERATING LLC

hazardous_liquid Incident — — September 17, 2013

Incident Information

Incident DateSeptember 17, 2013
OperatorENTERPRISE PRODUCTS OPERATING LLC
CommodityHVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI
Pipeline Typehazardous_liquid

Location

State
Coordinates36.08607, -101.04642

Cause

CauseEQUIPMENT FAILURE
Subcause"FAILURE OF EQUIPMENT BODY (EXCEPT PUMP), TANK PLATE, OR OTHER MATERIAL"

Casualties

Fatalities0
Injuries0

Costs

Property Damage$194,000
Emergency Response$15,000
Other Costs$7,000

Location Map

Incident Narrative

"ON 9/17/2013, A THIRD PARTY OPERATOR NOTIFIED ENTERPRISE PIPELINE CONTROL OF AN ICE BALL ON THE 10"" SOUTH LEG LOOP LINE VALVE. AN ENTERPRISE TECHNICIAN WAS DISPATCHED AND CONFIRMED A PIN HOLE LEAK ON THE VALVE BODY. THE PIPELINE WAS NOT RUNNING AT THE TIME. TWO VALVES WERE CLOSED TO BLOCK THE LEAKING SEGMENT AND FLARES WERE SET UP TO DISPLACE THE LINE. ONCE DISPLACED, THE LEAKING VALVE WAS CUT OUT AND REPLACED WITH ANOTHER VALVE. THE LINE WAS RETURNED TO SERVICE ON 9/26/2013 UPON COMPLETION OF THE REPAIRS. METALLURGICAL ANALYSIS IDENTIFIED THE FAILURE WAS CAUSED BY A POOR QUALITY WELD REPAIR. WELD DEFECTS THAT WERE OBSERVED INCLUDE A SMALL SECTION OF UNMELTED FILLER ROD OR WIRE THAT WAS INADVERTENTLY LEFT IN THE WELD, POROSITY, LACK OF FUSION, MECHANICAL NOTCHES, AND SEVERE GOUGING OF THE BASE METAL. THESE CONDITIONS CONSTITUTED LATENT DEFECTS THAT EVENTUALLY RESULTED IN CRACK PROPAGATION TO FAILURE AND LOSS OF CONTAINMENT. NOTE: THE NAME PLATE ON THE VALVE IDENTIFIES IT WAS REBUILT IN 1/17/1992 AND THE REPAIR PROCEDURES AND INSPECTION RECORDS ARE NOT AVAILABLE."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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