COLONIAL PIPELINE CO

hazardous_liquid Incident —

Incident Information

Report Date
OperatorCOLONIAL PIPELINE CO
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates32.78111, -88.04631

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON 8/7/12 AT 13:56 EMPLOYEES AT BOLIGEE DELIVERY DISCOVERED PRODUCT LEAKING FROM THE CONNECTION (1 1/2"" NIPPLE) TO THE BLOW DOWN VALVE ON THE LINE 1 TRAP BYPASS VALVE. THE EMPLOYEE NOTIFIED THE CONTROLLER AT 13:56, THE CONTROLLER CLOSED OUT THE DELIVERY AT 14:10 AND LEAKING IMMEDIATELY STOPPED. NOTIFICATION TO THE AREA OM WAS MADE AT 14:10. EMPLOYEES IMMEDIATELY BEGAN CLEAN UP AND REPAIR ACTIVITIES. REPAIR WAS COMPLETED AND LINE WAS RESTARTED AT 18:46. IT WAS DETERMINED THAT RELEASE IMPACTS WERE ISOLATED TO WITHIN AN APPROXIMATE 6' AREA AROUND THE VALVE AND EXTENDED TO AN APPROXIMATE DEPTH OF 4 TO 6 FEET. CLEAN UP CONTINUED THROUGH THE FOLLOWING DAY TO REMOVE SOIL IMPACTED BY THE RELEASE. AN ESTIMATED 20 TONS OF SOIL WERE EXCAVATED AROUND THE VALVE AND STOCKPILED FOR TRANSPORT AND OFF SITE DISPOSAL. THE RELEASE VOLUME ESTIMATE OF 9 GALLONS WAS DETERMINED FROM ANALYSIS OF THE IMPACTED SOIL. NO FREE PRODUCT WAS ENCOUNTERED OR RECOVERED. NEITHER GROUNDWATER OR SURFACE WATER WERE IMPACTED BY THE RELEASE.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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