MARATHON PIPE LINE LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorMARATHON PIPE LINE LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates38.85160, -90.08732

Cause

CauseINCORRECT OPERATION
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON AUGUST 1, 2012, LOCAL OPERATING PERSONNEL NOTICED A SMALL AMOUNT OF CRUDE OIL (0.013 GALLONS) ON THE CHIME OF TANK 1262 DURING A ROUTINE FACILITY CHECK. ON AUGUST 22, FURTHER INVESTIGATION REVEALED CRUDE OIL IN ONE OF THREE SOIL SAMPLES TAKEN WITHIN THE TANK DIKE, LAB ANALYSIS DETERMINED THE CRUDE TO BE FRESH. SUBSEQUENT SOIL SAMPLES HAVE NOT SHOWN INDICATIONS OF FRESH CRUDE. THE ORIGINAL ESTIMATED RELEASE VOLUME WAS CALCULATED USING DIMENSIONS OF IMPACTED SOIL FOUND VIA SOIL BORINGS. ANALYSIS OF IMPACTED SOILS LED TO A REVISED ESTIMATED RELEASE VOLUME. ALL IMPACTED SOIL WAS REMOVED AND DISPOSED. IN ATTEMPTS TO DISCOVER A RELEASE SOURCE, THE TANK WAS EMPTIED, TAKEN OUT OF SERVICE, AND CLEANED. THE TANK THEN UNDERWENT AN API 653 INSPECTION, AN MFL FLOOR SCAN, AND THE CRITICAL ZONE AND FLOOR WELDS WERE BLASTED AND NON-DESTRUCTIVELY TESTED. DURING THE VACUUM BOX TESTING ON SEPTEMBER 18, A SMALL HOLE WAS FOUND IN THE WELD OF A PATCH PLATE ON THE TANK FLOOR. THE CAUSE OF THE HOLE WAS DETERMINED TO BE A LACK OF FUSION OF THE WELD DUE TO INEFFECTIVE INSPECTION PROCEDURES IN 1992.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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