COLONIAL PIPELINE CO

hazardous_liquid Incident — — February 5, 2014

Incident Information

Incident DateFebruary 5, 2014
OperatorCOLONIAL PIPELINE CO
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates30.90931, -90.87143

Cause

CauseEQUIPMENT FAILURE
Subcause"FAILURE OF EQUIPMENT BODY (EXCEPT PUMP), TANK PLATE, OR OTHER MATERIAL"

Casualties

Fatalities0
Injuries0

Costs

Property Damage$200
Emergency Response$29,000
Other Costs$0

Location Map

Incident Narrative

"ON 5 FEBRUARY AT 0730, DURING A YARD CHECK, TECHNICIANS NOTED A PRODUCT SHEEN ON STANDING WATER IN THE LINE 2 AREA OF THE YARD. AN IMMEDIATE INVESTIGATION FOUND PRODUCT IN THE ACCESS WELLS IN THE VICINITY OF THE UNIT 3 CHECK VALVE. PRODUCT WAS REMOVED FROM THE ACCESS WELLS AND FROM THE STANDING WATER WITH APPROXIMATELY 40 GALLONS RECOVERED. THE CLEANUP WAS COMPLETED BY 0900 ON 2/5/14. MONITORING WAS CONDUCTED OVER THE NEXT 9 HOURS WITH NO NEW PRODUCT RELEASE OBSERVED. AT 0700 ON FEBRUARY 6TH A CREW ARRIVED AT THE STATION TO REMOVE THE WATER AND EXCAVATE AND INSPECT THE CHECK VALVES FOR UNITS 3 AND 4. A FLANGE ON THE INBOARD SPRING CANISTER FOR THE UNIT 3 CHECK VALVE WAS FOUND TO BE WEEPING. THE STATION WAS ISOLATED, DEPRESSURIZED, AND PERMANENT REPAIRS WERE MADE WITH COMPLETION TIME OF APPROXIMATELY 1100. NO OTHER LEAK SOURCES WERE FOUND. THE SPILL WAS REPORTED TO LOUISIANA DEQ ON 2/6/14 AT 7:54AM (REPORT #JI53 12539). SINCE THE EVENT DID NOT MEET NRC NOTIFICATION CRITERIA THE NRC WAS NOT NOTIFIED."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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