COLONIAL PIPELINE CO

hazardous_liquid Incident — — February 7, 2014

Incident Information

Incident DateFebruary 7, 2014
OperatorCOLONIAL PIPELINE CO
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates30.71126, -91.28299

Cause

CauseINCORRECT OPERATION
Subcause"VALVE LEFT OR PLACED IN WRONG POSITION, BUT NOT RESULTING IN A TANK, VESSEL, OR SUMP/SEPARATOR OVERFLOW OR FACILITY OVERPRESSURE"

Casualties

Fatalities0
Injuries0

Costs

Property Damage$0
Emergency Response$2,800
Other Costs$0

Location Map

Incident Narrative

"DURING AN INJECTION OF TRANSMIX, A MAINLINE UPSET OCCURRED THAT CAUSED PRESSURE TO INCREASE BACK INTO THE STATION. THE CONTROLLER DIRECTED THE LOCAL OPERATOR TO SHUT DOWN THE INJECTION AND THE OPERATOR CLOSED THE INJECTION VALVE CREATING A BLOCKED LINE CONDITION. LATER THE OPERATOR NOTED HIGH LEVEL ALARMS FOR THE INJECTION SUMP AND SENT A SECOND OPERATOR TO PUMP IT DOWN. AS THE SECOND OPERATOR HEADED TOWARD THE INJECTION SUMP, HE OBSERVED PRODUCT SPRAYING NEAR A METER. AT ABOUT THAT TIME, THE CONTROLLER DIRECTED THE FIRST OPERATOR TO RESTART THE INJECTION. WHEN THE INJECTION VALVE REOPENED THE PRODUCT STOPPED SPRAYING. IT WAS DETERMINED THAT THE PRODUCT HAD SPRAYED FROM A LOOSE INSPECTION CAP ON A CHECK VALVE FOR THE METER RUN THERMAL RELIEF DRAIN LINE. PRESSURE FROM THE TRANSMIX PUMP DURING THE BLOCKED LINE CONDITION HAD CAUSED THE THERMAL RELIEF TO ACTIVATE AND SEND PRODUCT TO THE INJECTION SUMP AS WELL AS VIBRATING THE CAP LOOSE WHICH ALLOWED THE RELEASE. THE CAP WAS TIGHTENED AND THE AREA CLEANED UP BY 18:00 THAT DAY."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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