SFPP, LP
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | SFPP, LP |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 38.56947, -121.52266 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
ON 1/8 A TANK CONTRACTOR NOTIFIED KM PERSONNEL OF A POSSIBLE RELEASE AT OUR SACRAMENTO STATION. AT 0957, KINDER MORGAN TECHNICIANS CONFIRMED THE RELEASE FROM FAILED VALVE PACKING ON MOV-1. THE ESTIMATED VOLUME OF THE RELEASE USING L-O&M 159 WAS ESTIMATED TO BE 9.3 GALLONS. THE LINE WAS SHUTDOWN, CA (AGENCY) LEAK NOTIFICATIONS WERE MADE AND AN INTERNAL ERL CALL WAS CONDUCTED. THE VALVE WAS REPACKED, IMPACTED SOIL WAS EXCAVATED AND PLACED INTO THREE LABELED DRUMS BY THE MAINTENANCE CREW AND THE EXCAVATION WAS BACKFILLED.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.