HOLLY ENERGY PARTNERS - OPERATING, L.P.

hazardous_liquid Incident —

Incident Information

Report Date
OperatorHOLLY ENERGY PARTNERS - OPERATING, L.P.
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates32.81300, -104.06118

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

14:00 RELEASE DISCOVERED BY HEP EMPLOYEE, CALLED INTO THE CONTROL CENTER, AND THE CONTROL CENTER SHUTDOWN THE PUMP. 14:05 CONTRACT CREWS WERE DISPATCHED TO HANDLE CLEAN-UP/ SOIL REMEDIATION. 14:15 THE SUCTION AND DISCHARGE LINES WERE ISOLATED (LEAK STOPPED AND CONTAINED) 15:13 REPORTED THE RELEASE TO NRC. 15:53 REPORTED THE RELEASE TO NM PUBLIC REGULATION COMMISSION (MIKE SMITH). 15:40 CONTRACT CREW AND BACKHOE AND ARRIVED ON-SITE. THE FREE PRODUCT DID FLOW ABOUT 50 FT (WEST) OUTSIDE OF THE STATION BUT WAS STILL CONTAINED ON THE HEP ROW. THE EQUIPMENT FAILURE WAS DUE TO IMPROPER REBUILD BY A CONTRACTOR. THE ROD BACKED OFF OF THE CROSSHEAD AND HIT THE LINER CAP. THE LOCKING NUT ON THE ROD/CROSSHEAD CONNECTION WAS NOT TIGHT. THE STATION VAPOR MONITOR DID NOT ALARM DUE TO HIGH WIND. THE PUMP WAS REPAIRED AND OPERATIONAL BY 1/30/2013.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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