CHEVRON PIPE LINE CO

hazardous_liquid Incident — — May 31, 2013

Incident Information

Incident DateMay 31, 2013
OperatorCHEVRON PIPE LINE CO
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates40.16005, -110.07770

Cause

CauseEQUIPMENT FAILURE
SubcausePUMP OR PUMP-RELATED EQUIPMENT

Casualties

Fatalities0
Injuries0

Costs

Property Damage$30,955
Emergency Response$36,916
Other Costs$0

Location Map

Incident Narrative

AT APPROXIMATELY 00:30 CDT ON 31MAY13, PERSONNEL AT THE MYTON STATION DISCOVERED A RELEASE OF AN ESTIMATED 10 BBLS CRUDE OIL TO CONCRETE CONTAINMENT AND LAND. THE CAUSE OF THE RELEASE WAS DETERMINED TO BE A FAILED GASKET ON THE INJECTION PUMP'S SUCTION STRAINER. THE PUMP WAS NOT RUNNING AND OIL CONTINUED TO LEAK FROM THE STRAINER UNTIL THE SEGMENT WAS ISOLATED AT 00:51. THE VOLUME RELEASED TO LAND OUTSIDE OF THE CONCRETE CONTAINMENT IS ESTIMATED TO BE 3 BBLS. FIELD TEAM PERSONNEL AND CONTRACTORS COMPLETED THE CLEANUP AND REPLACED THE FAULTY STRAINER GASKET.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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