CITGO PRODUCTS PIPELINE CO

hazardous_liquid Incident — — June 3, 2013

Incident Information

Incident DateJune 3, 2013
OperatorCITGO PRODUCTS PIPELINE CO
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates28.61171, -97.09409

Cause

CauseMATERIAL FAILURE OF PIPE OR WELD
SubcauseDESIGN-, CONSTRUCTION-, INSTALLATION-, OR FABRICATION-RELATED

Casualties

Fatalities0
Injuries0

Costs

Property Damage$82,000
Emergency Response$20,000
Other Costs$6,000

Location Map

Incident Narrative

ON MAY 30, 2013 CITGO RAN AN ILI COMBINATION TOOL FROM THE SAN ANTONIO RIVER CROSSING (2951+00) TO ITS VICTORIA STATION (4262+53). ON MONDAY, JUNE 3, 2013, FLIGHT SURVEILLANCE OBSSRVED BROWN VEGETATION AT THE LEAK SITE (3201+10) AT APPROXIMATLEY 12:24 PM. CITGO IMMEDIATLEY SHUTDOWN PUMPING ON THE PIPELINE. AT 12:54, CITGO PERSONNEL INVESTIGATED THE SITE AND OBSERVED A HEAVY DIESEL SMELL AND DEAD VEGATATION. THE MANUAL BLOCK VALVES AT KEMPER CITY RD AND AT THE SAN ANTONIO RIVER WERE CLOSED. PIPING AT THE LEAK SITE WAS EXCAVATED AND THE LEAK WAS TEMPORARY REPAIRED. THE LINE WAS SUBSEQUENTLY RESTARTED. ON TUESDAY, JUNE 4, 2013, THE PIPELINE WAS SHUTDOWN AND A 21-FOOT SECTION OF PIPE WAS REPLACED. THE PIPELINE WAS THEN RESTARTED. THE RELEASED VOLUME WAS ESTIMATED TO HAVE BEEN 200 BBLS DIESEL.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

Back to All Incidents More Incidents in