ONEOK NGL PIPELINE, LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorONEOK NGL PIPELINE, LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates36.60930, -98.51248

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ONEOK PIPELINE CONTROLLER NOTICED PRESSURE LOSS AT CABALLO EAGLE CHIEF INJECTION FACILITY AT 7:15 AM ON 2/12/2014 AND CONTACTED CABALLO PERSONNEL. NO PLANT PERSONNEL WERE ON LOCATION AT THE EAGLE CHIEF INJECTION PLANT AT THE TIME. CABALLO DISPATCHED PERSONNEL TO SITE. ONEOK CONTROLLER CONTACTED ONEOK OPERATIONS AND A ONEOK EMPLOYEE WAS ALSO DISPATCHED TO THE PLANT LOCATION. CABALLO EMPLOYEE ARRIVED AT APPROXIMATELY 8:15 AM AND IDENTIFIED THE 0.5 INCH DIAMETER PIPE-NIPPLE, CONNECTING THE PRESSURE TRANSMITTER TO THE DENSITOMITER ON THE ONEOK METERSKID, HAD COMPLETELY SEPARATED. THE CABALLO EAGLE CHIEF FACILITY WAS SHUT IN AND THE ONEOK METERSKID ISOLATED. ONEOK EMPLOYEE ARRIVED AT THE FACILITY AT APPROXIMATELY 8:45 AM. ONEOK EMPLOYEE REMOVED THE FAILED 0.5 INCH PIPE NIPPLE AND REPLACED WITH A NEW PIPE-NIPPLE THAT WAS SCHEDULE 160 PIPE AND APPROXIMATELY 0.5 INCHES LONGER FOR BETTER FITMENT. PIPE-NIPPLE THAT FAILED WAS SCHEDULE 80. AFTER COMPLETING THE INSTALLATIONOF THE NEW PIPE-NIPPLE, THE CABALLO EAGLE CHIEF PLANT WAS RESTARTED AND RESUMED INJECTION INTO THE ONEOK PIPELINE.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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