BKEP PIPELINE, LLC

hazardous_liquid Incident — — March 24, 2014

Incident Information

Incident DateMarch 24, 2014
OperatorBKEP PIPELINE, LLC
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates32.47599, -94.71869

Cause

CauseEQUIPMENT FAILURE
SubcauseTHREADED CONNECTION/COUPLING FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$350
Emergency Response$65,000
Other Costs$0

Location Map

Incident Narrative

ON MARCH 24, 2014 AT APPROXIMATELY 3:15 AM, A BKEP EMPLOYEE DISCOVERED CRUDE OIL LEAKING ON THE GROUND FROM A VALVE USED FOR COUPONS AND WATER DRAW DURING A LINE PURGE AT THE BKEP LONGVIEW STATION. THE EMPLOYEE STOPPED THE LEAK BY CLOSING A LINE VALVE. AT APPROXIMATELY 3:30 AM, THE EMPLOYEE AND TWO CONTRACTORS BEGAN CONTAINMENT AND SPILL RESPONSE OF LEAKED CRUDE OIL. NOTIFICATION OF THE INCIDENT WAS MADE TO THE NRC AND THE TEXAS RAILROAD COMMISSION . IT WAS ESTIMATED THAT 650 BARRELS OF CRUDE OIL WERE RELEASED DURING THE LEAK AND APPROXIMATELY 590 BARRELS OF CRUDE OIL WERE RECOVERED. AN INVESTIGATION WAS COMPLETED BY BKEP AND THE ROOT CAUSE OF THE LEAK WAS A CRACK ON THE THREADED CONNECTION OF THE TRAP VALVE. IN ADDITION, THE FAILED VALVE WAS SENT TO A LABORATORY FOR METALLURGICAL ANALYSIS. THE LABORATORY ANALYSIS REPORT POINTED TO MANUFACTURER CASTING DEFECTS WHICH RESULTED IN THE VALVE FAILURE.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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