"BUCKEYE PARTNERS, LP"

hazardous_liquid Incident — — September 2, 2015

Incident Information

Incident DateSeptember 2, 2015
Operator"BUCKEYE PARTNERS, LP"
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates42.11631, -72.58063

Cause

CauseCORROSION FAILURE
SubcauseEXTERNAL CORROSION

Casualties

Fatalities0
Injuries0

Costs

Property Damage$42,500
Emergency Response$32,000
Other Costs$0

Location Map

Incident Narrative

"AT 9/2/2015 12:50, LOCAL BUCKEYE OPERATIONS PERSONNEL EXCAVATED STAINED GRAVEL AROUND A CASING VENT AT A RAIL CROSSING IN SPRINGFIELD MA, ON THE SECTION OF LINE 915 RIGHT OF WAY BETWEEN AGNEW JUNCTION AND ATI DELIVERY FACILITY. THE PIPELINE WAS NOT RUNNING AT THE TIME OF DISCOVERY. IT HAS BEEN ESTIMATED THAT APPROXIMATELY 7.14 BARRELS OF TRANSMIX WAS RELEASED, AND 7 BARRELS HAS BEEN RECOVERED. THIS ESTIMATED VOLUME RELEASED, AND THE VOLUME RECOVERED WILL BE REEVALUATED WHEN A MORE ACCURATE VOLUME CAN BE CALCULATED. ALL FREE PRODUCT HAS BEEN RECOVERED, AND ALL EFFECTED STONES/SOIL HAS BEEN REMOVED. NO FURTHER REMEDIATION IS NECESSARY. THERE WERE NO INJURIES. AN INVESTIGATION INTO THE ROOT CAUSE IS ON-GOING. UPDATE ON 09/06/2016: 8.3 BARRELS OF TRANSMIX WAS RELEASED. ALL FREE PRODUCT WAS RECOVERED AND ALL AFFECTED SOIL WAS REMOVED. SITE CHARACTERIZATION ACTIVITIES ARE ONGOING. REMEDIATION ACTIVITIES, IF NECESSARY, WILL COMMENCE AFTER CHARACTERIZATION ACTIVITIES HAVE BEEN COMPLETED. THE METALLURGICAL CAUSE OF THE THROUGH-WALL LEAK WAS EXTERNAL PITTING CORROSION IN AN AREA WHERE THE PIPE COATING HAD FAILED."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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