"MAGELLAN PIPELINE COMPANY, LP"

hazardous_liquid Incident — — September 11, 2015

Incident Information

Incident DateSeptember 11, 2015
Operator"MAGELLAN PIPELINE COMPANY, LP"
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates41.69229, -90.31106

Cause

CauseEQUIPMENT FAILURE
SubcauseTHREADED CONNECTION/COUPLING FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$1,000
Emergency Response$40,000
Other Costs$0

Location Map

Incident Narrative

"A MAGELLAN MAINTENANCE CREW WAS WELDING A 2-INCH TOR ONTO THE #6-12 PIPELINE AT ALBANY JUNCTION IN PREPARATION TO LAUNCHING A PIG WHEN A NEARBY 1/2 INCH BALL VALVE ASSOCIATED WITH THE RELIEF TUBING FOR A MAINLINE VALVE FAILED. THE LINE WAS NOT RUNNING AT THE TIME AND THE RELEASE WAS QUICKLY CONTROLLED. THE DOWNSTREAM ROV WAS ALREADY CLOSED WHEN THE RELEASE OCCURRED SO THE PRESSURE RECEDED IN A SHORT AMOUNT OF TIME AND A PLUG WAS QUICKLY PLACED INTO THE FITTING. THE BALL VALVE THAT FAILED WAS APPROXIMATELY 20 FEET AWAY FROM THE TOR BEING INSTALLED. THE FAILED BALL VALVE WAS SENT TO A LABORATORY FOR ANALYSIS. THE LAB CONCLUDED THE VALVE SEPARATION RESULTED FROM A SHEAR OVERLOADING OF THE THREADS, MOST LIKELY DUE TO TEMPERATURE AND PRESSURE BUILD-UP FROM ELECTRICAL RESISTANCE HEATING DURING WELDING OF THE TOR."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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