"BUCKEYE PARTNERS, LP"

hazardous_liquid Incident — — September 23, 2015

Incident Information

Incident DateSeptember 23, 2015
Operator"BUCKEYE PARTNERS, LP"
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates42.11582, -72.58074

Cause

CauseCORROSION FAILURE
SubcauseEXTERNAL CORROSION

Casualties

Fatalities0
Injuries0

Costs

Property Damage$150,000
Emergency Response$120,000
Other Costs$0

Location Map

Incident Narrative

"AT 9/23/2015 14:00, LOCAL BUCKEYE OPERATIONS PERSONNEL WERE PERFORMING A PRESSURE TEST ON A REPAIRED PIPELINE IN SPRINGFIELD MA, ON THE SECTION OF LINE 915 RIGHT OF WAY BETWEEN AGNEW JUNCTION AND ATI DELIVERY FACILITY. THE PURPOSE OF THIS PRESSURE TEST WAS FOR VERIFICATION OF THE REPAIR OF NRC INCIDENT 1127403. UNSATISFACTORY PRESSURE TEST RESULTS PROMPTED AN INVESTIGATION, WHICH LED TO THE DISCOVERY OF THIS RELEASE. THE PIPELINE WAS NOT RUNNING AT THE TIME OF DISCOVERY. IT HAS BEEN ESTIMATED THAT APPROXIMATELY 2.9 BARRELS OF TRANSMIX WAS RELEASED, AND 2.9 BARRELS HAS BEEN RECOVERED. ALL FREE PRODUCT HAS BEEN RECOVERED, AND ALL EFFECTED STONES/SOIL HAS BEEN REMOVED. NO FURTHER REMEDIATION IS NECESSARY. THERE WERE NO INJURIES. AN INVESTIGATION INTO THE ROOT CAUSE IS ON-GOING. UPDATE ON 09/06/2016: THE METALLURGICAL CAUSE OF THE THROUGH-WALL LEAK WAS EXTERNAL PITTING CORROSION IN AN AREA WHERE THE PIPE COATING HAD FAILED."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

Back to All Incidents More Incidents in