JP ENERGY MARKETING, LLC

hazardous_liquid Incident — — September 28, 2014

Incident Information

Incident DateSeptember 28, 2014
OperatorJP ENERGY MARKETING, LLC
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates34.55307, -97.40303

Cause

CauseEQUIPMENT FAILURE
SubcauseMALFUNCTION OF CONTROL/RELIEF EQUIPMENT

Casualties

Fatalities0
Injuries0

Costs

Property Damage$0
Emergency Response$3,000
Other Costs$0

Location Map

Incident Narrative

A FAULTY RELAY SWITCH IN THE EXISTING PLC SCADA PACK THAT PROVIDES PERMISSIVE TO START/STOP THE DISCHARGE PUMP, SENSITIVE TO TANK LEVELS, CAUSED THE OUTBOUND DISCHARGE PUMP AND SCADA TANK LEVELS TO BE 100% INOPERABLE WHILE UPSTREAM VOLUMES CONTINUED TO FILL LIMITED TANK CAPACITIES AT THE STATION (THE LIMITED STORAGE CAPACITY WAS DUE TO THE TANK REPLACEMENT PROJECT WHERE THREE OF FIVE TANKS WERE OOS). A PIPELINE TECHNICIAN (RONNIE SMITH) NOTICED AN ABNORMAL TANK LEVEL INDICATION WHILE REVIEWING SCADALYNX ON HIS CELL PHONE, SO HE WENT TO INVESTIGATE THE ISSUE AND DISCOVERED THE RELEASE. RONNIE IMMEDIATELY NOTIFIED HIS SUPERVISOR AND WAS INSTRUCTED TO PROCEED TO THE UPSTREAM STATION (LONE GROVE) LOCATED 25 MILES AWAY TO ISOLATE FLOW INTO THE ELMORE STATION. THE RELEASE WAS STOPPED AT APPROXIMATELY 7:10PM. THE RELEASE WAS FULLY CONTAINED WITHIN SECONDARY CONTAINMENT AND RESPONSE/CLEANUP EFFORTS WERE DEPLOYED AT THIS TIME.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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