EXPLORER PIPELINE CO

hazardous_liquid Incident —

Incident Information

Report Date
OperatorEXPLORER PIPELINE CO
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates30.87850, -96.54234

Cause

CauseINCORRECT OPERATION
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON NOVEMBER 12, 2014 EXPLORER PIPELINE WAS COMPLETING SOME BASIC PUNCH LIST TASKS AT THE NEW HEARNE JUNCTION IN ROBERTSON COUNTY, TEXAS. A DOCUMENTED PRE-JOB MEETING WAS HELD WITH ALL THE PERSONNEL THAT OUTLINED THE TASKS TO BE COMPLETED ON NOVEMBER 12 IN PREPARATION FOR MORE DETAILED WORK ON NOVEMBER 14 WHEN THE PIPELINE WAS SCHEDULED TO BE SHUTDOWN. NONE OF THE DOCUMENTED PUNCH LIST TASKS COVERED IN THE NOVEMBER 12 MEETING INVOLVED ANY WORK WITH THE LAUNCHER DRAIN VALVE OR THE DRAIN VALVE PLUG. HOWEVER, AN OPERATOR QUALIFIED CONTRACTOR ELECTED TO REMOVE A ONE-HALF IN PLUG FROM A DRAIN VALVE THAT WAS NOT TO HAVE BEEN CONDUCTED UNTIL NOVEMBER 14. A RELEASE FROM THE VALVE WAS EXPERIENCED WHEN THE PLUG WAS REMOVED. THE PIPELINE WAS IMMEDIATELY SHUTDOWN AND RESPONSE EFFORTS WERE IMPLEMENTED. FREE-PHASE PRODUCT WAS RECOVERED AND ANY IMPACTED SOIL WAS EXCAVATED AND TESTED FOR PROPER MANAGEMENT. INTERVIEWS WITH ALL PARTIES INVOLVED, INCLUDING THE OWNER OF THE COMPANY, WERE CONDUCTED TO ASCERTAIN WHY THE CONTRACTOR FAILED TO FOLLOW CORRECT OPERATIONS OUTLINED AND DOCUMENTED IN THE PRE-JOB FOR NOVEMBER 12. THE INVESTIGATION CONFIRMED THE DIRECT CAUSE WAS THE CONTRACTOR WENT OUTSIDE THE CORRECT OPERATIONS DEFINED SCOPE OF WORK IN THE PRE-JOB AND ELECTED TO REMOVE THE PLUG.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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