"SHELL PIPELINE CO., L.P."

hazardous_liquid Incident — — April 11, 2016

Incident Information

Incident DateApril 11, 2016
Operator"SHELL PIPELINE CO., L.P."
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates29.85670, -94.99450

Cause

CauseMATERIAL FAILURE OF PIPE OR WELD
SubcauseORIGINAL MANUFACTURING-RELATED (NOT GIRTH WELD OR OTHER WELDS FORMED IN THE FIELD)

Casualties

Fatalities0
Injuries0

Costs

Property Damage$75,000
Emergency Response$50,000
Other Costs$0

Location Map

Incident Narrative

"NOTIFICATION TO VOLUNTARILY SHUT DOWN THE PIPELINE WAS DETERMINED BY THE GEN. MNGR, FACILITY MNGR & CONTROL CENTER MNGR. THEY WERE NOTIFIED BY OUR ROW TECH ON SITE OF A NEW PIPELINE LAY PARALLEL TO OUR PIPELINE. EXCAVATION HAD DISCOVERED A WATERY LIQUID AT THE SIX FT. OF DEPTH EXCAVATION. CONTROL CENTER SUPERVISOR INFORMED THE CONTROLLER TO SHUT DOWN THE E. HOU. TO PT. NECHES 20"" AND ISOLATE THE SEGMENT TO MOSS BLUFF P.S. OUR FIELD AND SME INTEGRITY GROUPS EXCAVATED AND INSPECTED THE PIPE. THEY COULD NOT DETERMINE THE SOURCE UNTIL PRESSURE WAS ADDED TO THE PIPELINE LATER THE 12TH. A PINHOLE WAS IDENTIFIED AT THE LONG SEAM OF THE PIPE. THE PIPELINE WAS DE-PRESSURED AND ISOLATED. THE COATING WAS REMOVED AND THE LONG SEAM WAS INSPECTED. NO CRACK IN THE LONG SEAM. A PINHOLE WAS FOUND. A FULL ENCIRCLEMENT SLEEVE WAS WELDED TO THE PIPELINE, COATED AND BACKFILLED. THE PIPELINE WAS RE-STARTED AT 08:00 4/13."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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