ENBRIDGE ENERGY, LIMITED PARTNERSHIP

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENBRIDGE ENERGY, LIMITED PARTNERSHIP
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates47.68990, -95.41192

Cause

CauseINCORRECT OPERATION
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON APRIL 23 AT APPROXIMATELY 10:10 AM CST, WHILE IN THE PROCESS OF REMOVING DRAIN LINE PIPING AT THE CLEARBROOK TERMINAL MANIFOLD AREA, OIL LEAKED PAST A 3"" DRAIN VALVE ON THE BOOSTER PUMP 3 AND 4 MANIFOLD HEADER, CAUSING AN ESTIMATED 10 BARRELS OF OIL TO LEAK OUT OF THE OPEN END OF THE PIPING AND THE COLD CUT THAT HAD BEEN MADE. THE TERMINAL GAUGER CONTACTED THE CONTROL CENTER AND REQUESTED THAT LINES 3 AND 4 ALONG WITH THE ASSOCIATED BOOSTER PUMPS 3 AND 4 BE SHUT DOWN. AS A PRECAUTION, ALL INCOMING LINES INTO THE CLEARBROOK TERMINAL WERE SHUT DOWN UNTIL THE SOURCE OF THE OIL COULD BE DETERMINED. THE INVESTIGATION REVEALED THAT THE 3"" DRAIN VALVE DID NOT PROPERLY SEAL, ALLOWING OIL TO FLOW PAST IT, ONTO THE GROUND. THE RESULTS OF THE FAILURE ANALYSIS REVEALED THAT A VARIETY OF DEBRIS WAS RESPONSIBLE FOR JAMMING THE DISC AND PREVENTING IT FROM BEING COMPLETELY CLOSED. THE ITEMS CONSISTED OF STAINLESS STEEL NUTS, BOLTS, AND WASHERS, A STAINLESS STEEL BRACKET, AND SOME IRON SULFIDE DEBRIS. THE SOURCE OF THE ITEMS AND HOW LONG THEY WERE STUCK IN THE VALVE IS UNKNOWN. AFTER REMOVING THE DEBRIS, THE VALVE WAS ABLE TO BE COMPLETELY CLOSED. APPROXIMATELY 40 CUBIC YARDS OF CONTAMINATED SOIL WAS DISPOSED OF TO AN APPROVED LANDFILL.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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