TALLGRASS PONY EXPRESS PIPELINE, LLC

hazardous_liquid Incident — — July 11, 2015

Incident Information

Incident DateJuly 11, 2015
OperatorTALLGRASS PONY EXPRESS PIPELINE, LLC
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates36.01195, -96.74166

Cause

CauseINCORRECT OPERATION
SubcauseTANK, VESSEL, OR SUMP/SEPARATOR ALLOWED OR CAUSED TO OVERFILL OR OVERFLOW

Casualties

Fatalities0
Injuries0

Costs

Property Damage$1,000
Emergency Response$1,800
Other Costs$0

Location Map

Incident Narrative

PRIOR TO THE OVERFILL EVENT AT CUSHING STATION THE TALLGRASS OPERATING CONTROL CENTER (OCC) HAD BEEN MAKING A DELIVERY TO SEPARATE STATIONS DURING WHICH A SPLIT FLOW OPERATION WAS IN PLACE FOR PONCA CITY CUSTOMER TO RECEIVE A CERTAIN RATE AND CUSHING STATION WOULD RECEIVE THE REMAINING BALANCE OF TOTAL FLOW COMING FROM STERLING. AS FLOW WAS TRANSFERRED FROM THE PONCA CITY STATION TO CUSHING STATION, AFTER DELIVERY WAS MADE AT PONCA CITY, THE IMPOSED FLOW LIMIT AT CUSHING STATION WAS NOT IMMEDIATELY CLEARED BY THE OPERATOR CAUSING PRESSURE TO RISE UNEXPECTEDLY. THE UNEXPECTED PRESSURE RISE DUE TO THE INCREASED FLOW ACTUATED THE THERMAL RELIEF VALVES AT THE STATION AND OIL FLOWED TO THE SUMP TANK AS DESIGNED. THE LEVEL TRANSMITTER OF THE CUSHING STATION SUMP TANK HAD BEEN DISCONNECTED DUE TO NUISANCE ALARMS THEREFORE THE OCC COULD NOT SEE THE LIQUID LEVEL IN THE TANK INCREASING RESULTING IN IT OVERFILLING. THE OVERFILLED TANK WAS PROMPTLY IDENTIFIED BY ON SITE PERSONNEL WHO NOTICED OIL ON THE GROUND. SUPPLEMENTAL REPORT SUBMITTED IN ORDER TO CLARIFY THAT THE ACCIDENT WAS DUE TO A FAILURE TO FOLLOW PROCEDURE. THIS HAS BEEN ADDRESSED IN PART G7.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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