BUCKEYE PARTNERS, LP

hazardous_liquid Incident —

Incident Information

Report Date
OperatorBUCKEYE PARTNERS, LP
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates40.60944, -74.24028

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON JULY 31, 2015 AT 00:50, A BUCKEYE LINDEN STATION EMPLOYEE WAS PERFORMING FACILITY SCHEDULED WALKING ROUNDS WHEN HE NOTICED DIESEL FUEL IN THE AREA OF THE UNIT #4 BOOSTER PUMP FOR LINE 603. THE LINE WAS SHUT DOWN AT THE TIME OF THE DISCOVERY. ALL FREE PRODUCT WAS CONTAINED WITHIN STATION PROPERTY. ALL FREE PRODUCT WAS RECOVERED BY 5:30 AM AND NO FURTHER REMEDIATION IS NECESSARY. THE TOTAL PRODUCT RECOVERED WAS 200 GALLONS. UPON INITIAL INVESTIGATION, THE SOURCE OF THE RELEASE APPEARED TO BE A FLANGE ON THE SUCTION SIDE OF UNIT #4. UNIT #4 WAS ISOLATED TO SECURE THE AREA. AT THAT TIME THE RELEASE DID NOT MEET THE THRESHOLD FOR A TELEPHONIC REPORT. AT 07:30, A TECHNICIAN CONDUCTED AN EVALUATION OF THE FAILURE. THIS EVALUATION REVEALED THE SOURCE OF THE RELEASE TO BE THE VALVE STEM PACKING, WHICH INCREASED THE ADDITIONAL ESTIMATED REPAIR COST CLOSE TO $50,000. OUT OF AN ABUNDANCE OF CAUTION, THE NRC WAS IMMEDIATELY NOTIFIED (NOTIFICATION #1124374). UPDATE 3/9/2017 GPS COORDINATES HAVE BEEN UPDATED. A BREAK DOWN OF THE VALVE STEM PACKING ALLOWED PRODUCT TO ESCAPE FROM THE VALVE BODY. THE VALVE WAS REPLACED WITH A CERTIFIED REPLACEMENT.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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