KIANTONE PIPELINE CORP

hazardous_liquid Incident —

Incident Information

Report Date
OperatorKIANTONE PIPELINE CORP
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates42.84905, -78.77696

Cause

CauseNATURAL FORCE DAMAGE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON 8/25/15 AT APPROXIMATELY 10:15AM A SMALL AMOUNT OF CRUDE OIL WAS DISCOVERED NEAR THE FILL LINE TO TANK 703 AT KIANTONE PIPELINE'S WEST SENECA TERMINAL. THE TANK HAD BEEN EMPTY AND OUT OF SERVICE FOR OVER A YEAR FOR AN API 653 INSPECTION. ALL OF THE TANK'S ANCILLARY PIPING HAD BEEN ISOLATED FROM THE TANK, BUT REMAINED FULL AND UNDER LOW PRESSURE (EST. 15 PSI.) UPON DISCOVERY OF THE OIL, FACILITY PERSONNEL QUICKLY EXCAVATED APPROXIMATELY 30 FEET OF THE BURIED FILL LINE BUT ONLY A SMALL AMOUNT OF OIL WAS ENCOUNTERED. UPON FURTHER INVESTIGATION AND TESTING, A SMALL BREAK WAS FOUND IN A MISSHAPED 2-INCH DRAIN-UP LINE CONNECTED TO THE TANK FILL LINE. THE BREAK WAS NOT INITIALLY APPARENT BECAUSE THE PIPE COATING SERVED TO MASK THE LEAK. SMES CONCLUDED THAT FREEZE/THAW CYCLES LIKELY PRECIPITATED THE DAMAGE TO THE IDLE DRAIN-UP LINE. SMES COULD NOT DETERMINE THE ULTIMATE STRESSOR THAT HAD CAUSED THE MISSHAPED PIPE TO FINALLY RELEASE (I.E. NO APPARENT MECHANICAL FORCE OR PRESSURE.) THE DAMAGED DRAIN UP LINE WAS DISCONNECTED AND REMOVED, AND A PRESSURE RATED CLAMP WAS INSTALLED OVER THE CONNECTION POINT.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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