MARATHON PIPE LINE LLC

hazardous_liquid Incident — — January 3, 2017

Incident Information

Incident DateJanuary 3, 2017
OperatorMARATHON PIPE LINE LLC
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates40.63107, -80.44046

Cause

CauseMATERIAL FAILURE OF PIPE OR WELD
Subcause"DESIGN-, CONSTRUCTION-, INSTALLATION-, OR FABRICATION-RELATED"

Casualties

Fatalities0
Injuries0

Costs

Property Damage$11,218
Emergency Response$29,651
Other Costs$0

Location Map

Incident Narrative

"ON JANUARY 3, 2017 PRODUCT WAS IDENTIFIED ON THE GRAVEL SURFACE AT MPL'S MIDLAND STATION PIPELINE MANIFOLD, NEAR THE RISER FOR THE TANK LINE. THE PIPELINE WAS EXCAVATED AND THE SOURCE OF THE RELEASE WAS DETERMINED TO BE A PINHOLE LEAK AT A WELD ON AN ELBOW OF A SEGMENT OF IDLE PIPING CONNECTED TO THE TANK LINE. THE LINE WAS REPAIRED BY REMOVING THE FAILED SEGMENT AND INSTALLING A FLANGE AND A BLIND. THE RELEASE WAS PROMPTLY CLEANED UP AND FOLLOWING REPAIR THE SYSTEM WAS RESTARTED PER SCHEDULE. MPL COMPLETED INVESTIGATIONS INTO THE RELEASE AND DETERMINED THAT THE WELD CONTAINED SIGNIFICANT MISMATCH (HIGH-LOW) AND ONLY A FEW CAP WELD PASSES. THE LACK OF A ROOT BEAD PROVIDED A CREVICE ON THE PIPE INTERIOR WHERE CREVICE CORROSION AND MICROBIOLOGICALLY INFLUENCED CORROSION (MIC) OCCURRED, RESULTING IN THE PINHOLE LEAK. 3/22/17: PART C.3.H WAS UPDATED. PART C.4. WAS UPDATED WITH YEAR ITEM INVOLVED IN ACCIDENT WAS INSTALLED. PART D.8. WAS UPDATED WITH FINAL COSTS. PART G UPDATED WITH CAUSE INFORMATION. 6/16/17: PART C, QUESTION 3A: THE NOMINAL DIAMETER OF PIPE WAS UPDATED TO 4 INCHES."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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