INLAND CORPORATION

hazardous_liquid Incident — — September 30, 2015

Incident Information

Incident DateSeptember 30, 2015
OperatorINLAND CORPORATION
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates39.78695, -84.16191

Cause

CauseEQUIPMENT FAILURE
SubcauseTHREADED CONNECTION/COUPLING FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$0
Emergency Response$35,000
Other Costs$0

Location Map

Incident Narrative

THE CONTROL CENTER WAS IN THE PROCESS OF REDIRECTING FLOW FROM ONE TERMINAL TO ANOTHER WHEN THE 3RD PARTY TERMINAL OPERATOR NOTICED THAT THE STRAINER ASSEMBLY HAD PRODUCT COMING FROM IT. THE PRODUCT POOLED IN A CONTAINMENT AREA AT THE MANIFOLD. THE MONTELLO CONTROL CENTER WAS NOTIFIED AND RESPONDED BY SHUTTING DOWN THE LINE. SXL SUPERVISION WAS NOTIFIED. SXL FIELD PERSONNEL AND OSRO'S RESPONDED TO ASSESS AND ADDRESS THE LEAK. 10 GALLONS OF GASOLINE WAS RECOVERED. IMPACTED SOIL WAS REMOVED.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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