HOLLY ENERGY PARTNERS - OPERATING, L.P.

hazardous_liquid Incident —

Incident Information

Report Date
OperatorHOLLY ENERGY PARTNERS - OPERATING, L.P.
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates32.84711, -104.39072

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

A PRELIMINARY FINDING OF SUMP OVERFILLED WAS INITIALLY REPORTED TO NRC. AFTER FURTHER INVESTIGATION IT WAS DETERMINED THAT THE SUMP DID NOT OVERFILL BUT IN FACT FOUR CORNERS UNIT 2 CASE THERMAL RELIEF VALVE OPENED, FLOWING PRODUCT INTO THE SUMP DRAIN LINE. THE PRODUCT FLOWING INTO THE SUMP, ALERTED CONTROLLER WITH A SUMP ALARM, SIMULTANEOUSLY BACK FLOWED ONTO UNIT 2 SKID THROUGH THE PUMP SKID'S SUMP DRAIN LINE. THE BACK FLOW OF PRODUCT ONTO THE SKID WAS DETERMINED TO BE FROM THE UNIT 2 SKID SUMP DRAIN LINE CHECK VALVE BEING HELD OPEN BY DEBRIS. THIS ALLOWED PRODUCT TO BE RELEASED ON TO THE PUMP SKID AND APPROXIMATELY 15 GALLONS OF DIESEL ON THE GROUND. THE CASE THERMAL RELIEF VALVE WAS REPLACED. THE SUMP DRAIN LINE AND CHECK VALVE WERE CLEANED OF DEBRIS. PIPELINE WAS PUT BACK INTO NORMAL SERVICE. CORRECTIVE ACTIONS: BI MONTHLY PUMP STATION PREVENTATIVE MAINTENANCE CHECKS TO INCLUDE THE SUMP DRAIN LINES ARE FREE OF DEBRIS, AND THE SUMP DRAIN LINE CHECK VALVES ARE WORKING PROPERLY.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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