EXPLORER PIPELINE CO

hazardous_liquid Incident —

Incident Information

Report Date
OperatorEXPLORER PIPELINE CO
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates30.26632, -95.35229

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON MARCH 31, 2016 AT APPROXIMATELY 18:55 CST A RELEASE OF ULTRA-LOW SULFUR DIESEL (ULSD) WAS IDENTIFIED TO BE ORIGINATING FROM A MAINLINE PUMP UNIT AT THE CONROE, TEXAS PUMP STATION. THE PIPELINE WAS IMMEDIATELY SHUTDOWN AND THE PUMP STATION WAS ISOLATED FROM THE MAINLINE PIPELINE BY THE TULSA, OKLAHOMA CONTROL CENTER. EXTERNAL AND INTERNAL RESPONSE RESOURCES WERE NOTIFIED TO RESPOND. PRIOR TO THE SHUTDOWN OF THE PIPELINE AND STATION THE CASE PRESSURE WAS 620.4 PSI AND THE DISCHARGE PRESSURE WAS 615.9 PSI. UPON ARRIVAL AT THE PUMP STATION THE SOURCE OF THE RELEASE WAS IDENTIFIED TO BE A THREE-QUARTER INCH 316 SEAMLESS STAINLESS STEEL TUBING AND FITTING UTILIZED FOR THE MAINLINE UNIT NUMBER 2 SEAL FLUSH SYSTEM. ON APRIL 1, 2016 AT 13:18 CST THE PIPELINE WAS RESTARTED, BUT THE CONROE PUMP STATION WAS LEFT ISOLATED FROM THE PIPELINE. ON APRIL 5, 2016 AT 11:45 CST THE CONROE PUMP STATION WAS UNISOLATED FROM THE PIPELINE AND STARTED AT 11:52 CST. THE TUBING AND FITTING WERE BOTH PHOTO DOCUMENTED BY EXPLORER AND PHMSA. THE TUBING AND FITTING WERE SUBMITTED TO A THIRD-PARTY FOR A FAILURE ANALYSIS. A COPY OF THE THIRD-PARTY FAILURE ANALYSIS WAS PROVIDED TO PHMSA. ALL IMPACTED SOIL FROM THE REMEDIATION WAS EXCAVATED, TESTED AND WAS PROPERLY HANDLED.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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