SHELL PIPELINE CO., L.P.
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | SHELL PIPELINE CO., L.P. |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 30.01665, -90.84478 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
TK 108 MIXER FAILED AT THE THRUST BEARING CAUSING A SEAL LEAK. SECONDARY SEAL SET TO INSURE LEAKAGE STOPPED. NORMAL OPERATION WAS ALLOWED TO RESUME UNTIL A REPLACEMENT MIXER IS AVAILABLE AND TANK VOLUME PUMPED OUT BELOW THE MIXER FLANGE. MIXER TO BE REPLACED WITH REPLACEMENT. INSPECTION OF THE MIXER WILL FOLLOW. MIXER REPLACED WEEK OF JULY 25TH. NO ADDITIONAL INFORMATION FOUND FOLLOWING THE REPLACEMENT OF THE MIXER. THE COMMODITY SIDE OF THE MIXER INSIDE OF THE TANK WAS IN GOOD CONDITION. VIBRATION IDENTIFIED ALLOWING THE SHAFT TO MOVE AXIALLY. THE THRUST BEARING FAILED CAUSING THE SEAL LEAK TO THE TANK DIKE AREA.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.