"MAGELLAN PIPELINE COMPANY, LP"

hazardous_liquid Incident — — February 18, 2018

Incident Information

Incident DateFebruary 18, 2018
Operator"MAGELLAN PIPELINE COMPANY, LP"
CommodityREFINED AND/OR PETROLEUM PRODUCT (NON-HVL) WHICH IS A LIQUID
Pipeline Typehazardous_liquid

Location

State
Coordinates35.30939, -94.39479

Cause

CauseEQUIPMENT FAILURE
SubcauseNON-THREADED CONNECTION FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$100
Emergency Response$68,000
Other Costs$0

Location Map

Incident Narrative

"DURING THE DAILY FACILITY INSPECTION, A TECHNICIAN DISCOVERED THE 2"" BALL VALVE ON THE LIQUID BOTTOM SAMPLER WAS LEAKING. THE SAMPLER IS LOCATED BETWEEN THE RECEIVE TRAP AND THE PROVER. OPERATIONS CONTROL WAS NOTIFIED TO SHUT DOWN THE MAINLINE AND LOCAL PERSONNEL ISOLATED THE LINE SEGMENT CONTAINING THE BALL VALVE. THE RELEASE WAS CONTAINED AND AFFECTED STORM WATER AND SOIL WAS PROPERLY DISPOSED. A PORTION OF THE GASOLINE VOLUME LOST IS ATTRIBUTED TO EVAPORATION. SOIL TESTING RESULTS IN THE IMPACTED AREA WERE BELOW EPA/ADEQ SOIL SCREENING LEVEL. APPROVAL WAS RECEIVED FROM THE STATE THAT INDICATED NO FURTHER SOIL REMEDIATION IS REQUIRED. THE BALL VALVE AND LIQUID SAMPLER WERE REMOVED AND A BLIND FLANGE WAS INSTALLED. FROM PRELIMINARY INVESTIGATION, IT APPEARS THE O-RING WAS DAMAGED UPON INSTALLATION BY THE MANUFACTURER. APPROXIMATELY 70 CUBIC YARDS OF SOIL WERE REMEDIATED"

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

Back to All Incidents More Incidents in