"ONEOK NGL PIPELINE, LLC"

hazardous_liquid Incident — — February 26, 2018

Incident Information

Incident DateFebruary 26, 2018
Operator"ONEOK NGL PIPELINE, LLC"
CommodityHVL OR OTHER FLAMMABLE OR TOXIC FLUID WHICH IS A GAS AT AMBI
Pipeline Typehazardous_liquid

Location

State
Coordinates32.40217, -102.69515

Cause

CauseINCORRECT OPERATION
SubcauseEQUIPMENT NOT INSTALLED PROPERLY

Casualties

Fatalities0
Injuries0

Costs

Property Damage$300
Emergency Response$150
Other Costs$0

Location Map

Incident Narrative

"AT APPROXIMATELY 12:10 ON 2/26/2018, THE ONEOK PIPELINE CONTROL CENTER RECEIVED A CALL FROM A DCP EMPLOYEE AT THE DCP ANDREWS METER STATION CONNECTION, ADVISING OF VAPOR RELEASE ON ONEOK'S METER PIPING. THIS CONNECTION IS NOT ACTIVE AT THIS TIME. ONEOK FIELD EMPLOYEES RESPONDING TO THE CALL DETERMINED THE LEAK ORIGINATED BETWEEN TWO FLANGES WHERE A FLEXITALLIC GASKET AND A FIBER INSULATOR GASKET HAD BEEN IMPROPERLY INSTALLED TOGETHER. THE INSULATOR GASKET HAD FAILED AND WAS THE CAUSE OF THE LEAK. THE PIPING WAS ISOLATED AND DE-PRESSURED. THE FLEXITALLIC GASKET WAS REMOVED AND A NEW INSULATOR GASKET INSTALLED BETWEEN THE FLANGES AND RETURNED TO NORMAL OPERATIONS. ONEOK'S INVESTIGATION DETERMINED THE GASKETS HAD BEEN IMPROPERLY INSTALLED IN 2012 BY THE PREVIOUS OPERATOR OF THE ASSET."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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