"MEDALLION OPERATING COMPANY, LLC"

hazardous_liquid Incident — — November 19, 2018

Incident Information

Incident DateNovember 19, 2018
Operator"MEDALLION OPERATING COMPANY, LLC"
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates32.21265, -101.54602

Cause

CauseMATERIAL FAILURE OF PIPE OR WELD
SubcauseORIGINAL MANUFACTURING-RELATED (NOT GIRTH WELD OR OTHER WELDS FORMED IN THE FIELD)

Casualties

Fatalities0
Injuries0

Costs

Property Damage$10,000
Emergency Response$1,000
Other Costs$0

Location Map

Incident Narrative

"ON MONDAY, NOVEMBER 19, 2018, AT 12:30 P.M. LOCAL TIME, MEDALLION OPERATING'S HOWARD FACILITY, KNOWN AS THE HOWARD STATION, IN HOWARD COUNTY, TEXAS, DEVELOPED A PIN HOLE LEAK ON A 3"" CARBON STEEL ELBOW. THE INCIDENT OCCURRED AT A 3"" BYPASS AROUND AN ACTUATED VALVE WITHIN THE STATION PIPPING. A MEDALLION PIPELINE TECHNICIAN IMMEDIATELY CONTACTED MEDALLION'S CONTROL CENTER PROVIDING NOTIFICATION OF THE LEAK AND REQUESTED THE FACILITY TO BE PLACED IN BYPASS. THE BYPASS WAS COMPLETED AT 12:35 P.M. LOCAL TIME, WHICH SHUT OFF THE FLOW OF OIL TO THROUGH THE AFFECTED PIPING. A TOTAL OF 2 BBLS WAS RELEASED AND APPROXIMATELY 1.5 BBL WAS RECOVERED BY VACUUM TRUCK. THE REMAINING CONTAMINATED SOILED WAS TREATED IN-PLACE AND HAS BEEN REMEDIATED BELOW CLOSURE LEVELS. AT APPROXIMATELY 13:30 P.M. LOCAL TIME, MEDALLION'S CONTRACTORS ARRIVED ON LOCATION TO START REPAIRS. THE ELBOW WAS COLD CUT ALONG WITH ADJACENT PIPING AND VISUALLY INSPECTED. THE VISUAL INSPECTION INDICATED THE 3"" ELBOW HAD DEVELOPED A SMALL PINHOLE AND MEDALLION HAS SUBMITTED THE AFFECTED ELBOW AND PIPING TO AN INDEPENDENT SUBJECT MATTER EXPERT (METALLURGIST) FOR REVIEW AND ANALYSIS. THE RESULTS OF THE ANALYSIS ARE PENDING AT THE TIME OF THIS INITIAL REPORT. THE REMAINING SECTION OF PIPING ON THE 3"" BYPASS WAS REMOVED AND REPLACED WITH NEW MATERIAL. AT 19:10 P.M. LOCAL TIME, THE REPAIRS WERE COMPLETED AND THE STATION (AFFECTED PIPING) WAS PLACES BACK IN SERVICE. AN SUPPLEMENT WILL BE PROVIDED, AFTER THE METALLURGIST REPORT IS RECEIVED AND REVIEWED. UPDATE: THE INVESTIGATION AND METALLURGICAL REPORT INDICATED MORE THAN ONE FACTOR ATTRIBUTED TO THE ACCIDENT. EACH OF THE FOLLOWING HAS BEEN IDENTIFIED AS A CONTRIBUTING FACTOR, A METALLURGICAL DEFECT IN THE 90 IN THE HEAT AFFECTED ZONE OF THE WELD, WATER / OIL INTERFACE CORROSION AND THE METALLURGICAL REPORT INDICATED A POTENTIAL CAUSE WAS DUE TO EROSION CORROSION. DUE TO THE UNIQUE CONTRIBUTING FACTORS THE FAILURE OF THE 3"" 90, MEDALLION ADDED AN 3"" VALVE TO THE BYPASS LINE TO ELIMINATE A DEAD LEG IN THE PIPING WHEN THE BYPASS IS NOT IN USE."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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