MARATHON PIPE LINE LLC

hazardous_liquid Incident — — December 24, 2018

Incident Information

Incident DateDecember 24, 2018
OperatorMARATHON PIPE LINE LLC
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates30.01333, -90.86024

Cause

CauseCORROSION FAILURE
SubcauseINTERNAL CORROSION

Casualties

Fatalities0
Injuries0

Costs

Property Damage$255,000
Emergency Response$803,000
Other Costs$0

Location Map

Incident Narrative

"ON DECEMBER 24, A MPL TECHNICIAN DISCOVERED A RELEASE OF CRUDE OIL WITHIN THE ST. JAMES CAPLINE STATION. ALL PRODUCT WAS CONTAINED ON-SITE AND CLEANED UP PROMPTLY. RELEASE VOLUME IS 30 BARRELS BASED UPON AMOUNT OF CRUDE OIL COLLECTED AND ESTIMATED AMOUNT OF OIL CONTAMINATED SOIL. VALVE HAS BEEN REMOVED,NEW VALVE HAS BEEN INSTALLED, AND THE SYSTEM HAS BEEN RETURNED TO NORMAL OPERATIONS. FOLLOWING METALLURGICAL ANALYSIS, THE CAUSE HAS BEEN DETERMINED TO BE MICROBIOLOGICAL INTERNAL CORROSION. NOTE: INITIAL NRC REPORT (#1233864) WAS MADE ON 12/24/2018 AT 15:04 CST. THE 48 HOUR UPDATE REPORT (#1233952) WAS MADE ON 12/26/2018 AT 14:53 CST. 1/18/19 UPDATE- PART H-NARRATIVE 2/13/19 UPDATE- PART D-COSTS 3/21/19 UPDATE- PART D-COSTS AND PART H - NARRATIVE"

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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