DCP MIDSTREAM

hazardous_liquid Incident —

Incident Information

Report Date
OperatorDCP MIDSTREAM
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates31.80026, -103.13523

Cause

CauseINCORRECT OPERATION
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

2 DCP EMPLOYEES REPAIRED A SMALL LEAK AT WINK PUMP STATION ON PUMP P310 SEAL. AFTER REPAIR WAS COMPLETED THE PUMP WAS PRESSURED UP TO CHECK FOR LEAKS. WHEN PRESSURE REACHED 1251 PSI THE 3/4 INCH SEAL FLUSH TUBING FERREL FAILED DUE TO IMPROPER TORQUING. THE ON SITE ESD WAS IMMEDIATELY ACTIVATED BY ONE OF THE EMPLOYEES ON LOCATION AS SOON AS THE RELEASE OCCURRED. THE PUMP WAS NOT IN OPERATION AT THE TIME OF THE RELEASE. EMPLOYEES WERE LEAK CHECKING AFTER REPAIR WAS COMPLETED. NOTE: 11/9/17 CHANGED FROM G8 OTHER TO G6 EQUIPMENT FAILURE AT THE TRRC INSPECTOR STEVE BURNETT'S REQUEST. 2/5/18 CHANGED FROM G6 EQUIPMENT FAILURE TO G7 INCORRECT OPERATION. CORRECTIVE ACTION: EMPLOYEES WILL RECEIVE RETRAINING ON SMALL DIAMETER METAL TUBING AND FITTING INSTALLATION. ON 1/29/18 DCP MIDLAND NGL TECH'S AND MEASUREMENT TECH RECEIVED AND COMPLETED SWAGELOK 4 HOUR INSTALLATION & TUBE FITTING TRAINING.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

Back to All Incidents More Incidents in