ENBRIDGE ENERGY, LIMITED PARTNERSHIP

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENBRIDGE ENERGY, LIMITED PARTNERSHIP
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates41.51465, -87.45005

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON DECEMBER 9, 2017 AT 9:36 CST, LINE 78 WAS SHUTTING DOWN DUE TO AN ODOR COMPLAINT UPSTREAM OF GRIFFITH TERMINAL. AT 9:38 CST VALVE 79.67-78-V-1 WAS CLOSING AND PLM PERSONNEL WHO WERE ONSITE NOTICED THAT CRUDE OIL WAS BEING RELEASED FROM THE STEM AREA. APPROXIMATELY 20 GALLONS OF CRUDE OIL WAS RELEASED DURING THE TRAVEL PHASE OF THE VALVE. THE RELEASE WAS CAUSED BY THE STUDS BEING LOOSE AT THE CUPOLA ON THE VALVE. THE REPAIR INVOLVED REMOVING THE CONNECTION TO INSPECT THE SURFACES AND O-RING. NO ISSUES WERE SEEN, SO IT WAS REASSEMBLED AND ALL STUDS WERE TIGHTENED. TECHNICIAN CONFIRMED THAT ODOR COMPLIANT WAS NOT ENBRIDGE RELATED AND FOUND WHAT APPEARED TO BE MARINE OIL IN THE LANDOWNERS SUMP SYSTEM. APPROXIMATELY 30 YARDS OF CONTAMINATED SOIL WAS REMOVED FROM RELEASE SITE.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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