ENTERPRISE PRODUCTS OPERATING LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENTERPRISE PRODUCTS OPERATING LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates29.91050, -94.00990

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON DECEMBER 18TH, 2017 AT APPROXIMATELY 12:00 PM AN OPERATOR MAKING ROUNDS AT THE NORTH PORT ARTHUR FACILITY DISCOVERED PRODUCT LEAKING FROM THE 1/2"" BLEEDER VALVE ON THE DENSITOMETER ON THE CONNECTION TO THE COLONIAL DISTILLATE PIPELINE. THIS LEAK WAS REPORTED TO THE TEXAS RAILROAD COMMISSION ON DECEMBER 18TH, 2017 AT 13:38 (INCIDENT #1690). APPROXIMATELY 10 GALLONS OF JET FUEL WERE RELEASED. THE LEAK WAS CONTAINED TO OPERATOR PROPERTY AND NO PRODUCT CAME IN CONTACT WITH ANY WATERWAYS. THE AREA WAS CLEANED UP, THE BLEEDER VALVE WAS REMOVED AND THREAD SEALANT WAS RE-APPLIED, THE VALVE WAS RE-INSTALLED, AND THE DENSITOMETER WAS RETURNED TO SERVICE. ACCIDENTS/INCIDENTS CAUSED BY EQUIPMENT FAILURE ARE TRENDED AND TRACKED IN OUR OPERATIONAL CONTAINMENT PROGRAM.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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