GENESIS PIPELINE USA, L.P.
hazardous_liquid Incident — — June 19, 2018
Incident Information
| Incident Date | June 19, 2018 |
| Operator | GENESIS PIPELINE USA, L.P. |
| Commodity | CRUDE OIL |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 31.53802, -90.45444 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | NON-THREADED CONNECTION FAILURE |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | $71,490 |
| Emergency Response | $17,736 |
| Other Costs | $0 |
Location Map
Incident Narrative
GENESIS RECEIVED A CALL FROM A NEIGHBORING PIPELINE OPERATOR THAT THEIR AERIAL PATROL SPOTTED OIL ON THE GROUND NEAR THE GENESIS ROW SOUTH OF BROOKHAVEN, MS. THE PIPELINE WAS SHUT DOWN AND PERSONNEL WERE DISPATCHED TO LOCATION AND ARRIVED TO FIND PRODUCT SPRAYING FROM A VALVE. OSRO CALLED FOR CLEAN-UP. INSPECTION OF THE VALVE SHOWED THAT IT WAS A REFURBISHED VALVE THAT WAS NOT INSTALLED PROPERLY BY THE CONTRACTOR IN 2006. IT WAS DISCOVERED THAT THE VALVE BONNET FLANGE DID NOT HAVE A O-RING IN THE O-RING GROOVE. IN ITS PLACE, THE CONTRACTOR HAD USED A SILICONE SEALANT INSTEAD OF USING THE MANUFACTURER'S RECOMMENDED PARTS. THE SILICONE USED HAD BECOME BRITTLE AND CRACKED OVER TIME CAUSING THE BONNET FLANGE TO LEAK. THE VALVE WAS REPAIRED AND THE PIPELINE WAS PLACED BACK INTO SERVICE. SUPPLEMENTAL (08/06/18) - UPDATE TO NRC NUMBER IN PART A. UPDATE TO LATITUDE NUMBER TO CORRECT TYPO IN PART A. ADDITIONAL TIMELINE DETAILS: 6/19/18 14:01 - DENBURY PILOT SPOTS OIL ON THE ROW AND CALLS DENBURY TO NOTIFY. DENBURY IN TURN CALLS THEIR FIELD OPERATOR TO TRAVEL TO THE LOCATION AND ASSESS THE POTENTIAL RELEASE. 14:40 - DENBURY FIELD PERSONNEL ARRIVES AT THE LOCATION AND CALLS GENESIS FIELD PERSONNEL TO REPORT IT IS A GENESIS PIPE (VALVE) LEAKING. 14:45 - GENESIS PERSONNEL ARRIVES AT THE LOCATION AND CALLS GENESIS PIPELINE MANAGER TO REPORT THAT A GENESIS PIPE IS LEAKING. THE GENESIS PIPELINE MANAGER BEGINS COLLECTING INFORMATION ABOUT THE PIPELINE AND VOLUME RELEASED. 15:12 - GENESIS PIPELINE MANAGER CALLS GENESIS INTERNAL NOTIFICATION HOTLINE TO REPORT THE RELEASE. 3RD PARTY CONTRACTOR (WITT OBRIENS) MAKES NOTIFICATION CALLS TO OSROS AND GENESIS CORPORATE PERSONNEL. 16:03 - GENESIS (BY WAY OF WITT O'BRIENS) NOTIFIES NRC OF THE RELEASE. 6/23/18 THE VALVE IN QUESTION IS REPAIRED AND THE PIPELINE IS PLACED BACK INTO SERVICE. ONE UPSTREAM VALVE WAS INSPECTED AND FOUND TO BE IN A SIMILAR CONDITION WITH VERY LITTLE PRODUCT LEAKING. THE VALVE WAS MONITORED DURING PRODUCT TRANSFER WITH APPROPRIATE CONTAINMENT APPLIED IN ORDER TO CATCH ANY VOLUME OF PRODUCT THAT MAY COME OUT OF THE BONNET. THE AMOUNT OF PRODUCT COLLECTED DURING THE TRANSFER FROM THIS VALVE WAS APPROXIMATELY ONE OUNCE. THE THIRD AND FINAL VALVE ON THIS SEGMENT WAS INSPECTED AND FOUND TO BE IN GOOD CONDITION AND WITH APPROPRIATE MANUFACTURER PARTS. 6/28/18 THE UPSTREAM VALVE WAS CLEANED UP AND REPAIRED ON 6/28.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.