WESTERN REFINING PIPELINE, LLC

hazardous_liquid Incident — — July 24, 2018

Incident Information

Incident DateJuly 24, 2018
OperatorWESTERN REFINING PIPELINE, LLC
CommodityCRUDE OIL
Pipeline Typehazardous_liquid

Location

State
Coordinates35.73283, -107.74805

Cause

CauseEQUIPMENT FAILURE
SubcauseTHREADED CONNECTION/COUPLING FAILURE

Casualties

Fatalities0
Injuries0

Costs

Property Damage$100
Emergency Response$0
Other Costs$0

Location Map

Incident Narrative

ONE INCH NIPPLE ON DISCHARGE LINE DRAIN BROKE THE THREADS AND CAUSED A SPILL AT HOSPAH STATION. APPROXIMATELY 3.8 BBLS WERE SPILLED. 3.40 BBLS WERE RECOVERED FROM THE ENVIRONMENTAL SKID, AND 16 GALLONS SPRAYED ONTO THE GROUND SURFACE. PUMPS WERE IMMEDIATELY SHUT DOWN AND LEAKING NIPPLE WAS ISOLATED. THE BROKEN NIPPLE HAS BEEN SENT FOR METALLURGICAL ANALYSIS. THE PART G8 APPARENT CAUSE SELECTION WILL BE CHANGED TO PART G6 ONCE WE RECEIVE THE METALLURGICAL ANALYSIS, COMPLETED. A FAILURE ANALYSIS CONDUCTED ON THE LEAKING THREADED VERTICAL PIPE NIPPLE REVEALED THAT A CRACK ORIGINATED AT THE ROOT OF AN UNENGAGED THREAD. THE FAILURE MECHANISM WAS METAL FATIGUE LIKELY DUE TO VIBRATIONAL TENSILE STRESSES ORIGINATING FROM THE NEARBY MAINLINE PUMP #1. EXTERNAL TENSILE STRESSES WERE EXACERBATED BY THE WEIGHT OF A BALL VALVE ATTACHED TO THE HORIZONTAL PIPE NIPPLE ATTACHED TO THE 90-DEGREE ELBOW.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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